ASN Wikibase Occurrence # 312368
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Thursday 13 April 2023 |
Time: | 12:00 LT |
Type: | Pipistrel Sinus 912 |
Owner/operator: | |
Registration: | N413EK |
MSN: | 1025 SFNM 912 LSA |
Year of manufacture: | 2020 |
Total airframe hrs: | 309 hours |
Engine model: | Rotax 912 UL |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Ford Airport (IMT/KIMT), Iron Mountain, MI -
United States of America
|
Phase: | Standing |
Nature: | Private |
Departure airport: | Kingsford , MI |
Destination airport: | Menominee Marinette Twin County Airport, MI (KMNM) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot stated the engine lost power as he increased power for takeoff. The engine could not be restarted, and the airplane was pushed off the runway onto a taxiway. The pilot allowed the engine to cool and then restarted the engine. The engine ran smoothly for about one minute. When engine power was increased above 4,000 rpm, the engine lost power again. The pilot performed 2 additional engine starts, which also resulted in the engine quitting above 4,000 rpm. The pilot then noticed white smoke emitting from the engine compartment. A fire ensued that resulted in substantial damage to the motorglider.
Postaccident examination of the engine revealed that the right carburetor bowl cover was attached to the carburetor bowl but the carburetor bowl cover retention clip was not in its secure position on the bowl cover. The left carburetor bowl cover was missing and was not recovered; it most likely fell out of the motorglider or was dislodged from the airplane when the fire was being extinguished. An unsecured bowl cover would have allowed fuel to leak onto hot exhaust pipes, resulting in a fire.
Neither carburetor had optional carburetor drip trays installed to mitigate the risk of an engine fire from fuel leaking onto the engine exhaust from the carburetors by directing it away from the exhaust and overboard, which may have prevented the accident.
Engine logbook entries showed that the carburetor bowl covers were removed during recent maintenance. It is likely that the covers were not properly reinstalled during that maintenance.
Probable Cause: The failure of maintenance personnel to properly secure the left carburetor bowl cover, which resulted in an engine fire before takeoff.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN23LA165 |
Status: | Investigation completed |
Duration: | 11 months |
Download report: | Final report |
|
Sources:
NTSB CEN23LA165
https://flightaware.com/live/flight/N413EK Location
Revision history:
Date/time | Contributor | Updates |
10-May-2023 21:26 |
Captain Adam |
Added |
04-Apr-2024 09:49 |
ASN Update Bot |
Updated [Time, Cn, Operator, Other fatalities, Departure airport, Source, Narrative] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation