ASN Wikibase Occurrence # 314620
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Date: | Thursday 15 July 2010 |
Time: | 15:30 LT |
Type: | Beechcraft A36 |
Owner/operator: | Connelly Equipment Rental Co LLC |
Registration: | N4153Q |
MSN: | E-2687 |
Year of manufacture: | 1992 |
Total airframe hrs: | 5256 hours |
Engine model: | Continental IO-550 SERIES |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | None |
Category: | Accident |
Location: | Las Vegas, Nevada -
United States of America
|
Phase: | Standing |
Nature: | Private |
Departure airport: | Las Vegas, NV |
Destination airport: | San Diego-Gillespie Field, CA (SEE/KSEE) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The passenger reported that after loading the baggage, she and the pilot got into the airplane and the pilot attempted to start the engine. According to the passenger, the engine would not start and described it as running rough. When the engine finally started, the pilot attempted to move the airplane forward but realized the wheel chocks were still securing it. The passenger offered to help and exited the airplane. Without receiving instruction, she crawled under the right wing and forward to the right side of the nose of the airplane. As she leaned in to remove the chocks, the propeller struck her. After a Federal Aviation Administration inspector described a preflight inspection to the passenger, she stated that she could not recall seeing the pilot ever perform this action. The pilot reported that after he realized the chocks were still securing the airplane he did not want to shut down the engine due to the high outside air temperature. In the recommendation section of the National Transportation Safety Board 6120.1 form, the pilot stated that the accident could have been prevented by not allowing the passenger to exit the airplane while the engine was running.
Probable Cause: The passenger's failure to maintain clearance from a turning propeller. Contributing to the accident was the pilot's inadequate preflight inspection.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR10LA352 |
Status: | Investigation completed |
Duration: | 1 year and 2 months |
Download report: | Final report |
|
Sources:
NTSB WPR10LA352
Location
Revision history:
Date/time | Contributor | Updates |
02-Jun-2023 19:00 |
ASN Update Bot |
Added |
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