Accident Varga 2150A Kachina N5601G,
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ASN Wikibase Occurrence # 318436
 
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Date:Thursday 27 July 2023
Time:12:33 LT
Type:Silhouette image of generic MOR2 model; specific model in this crash may look slightly different    
Varga 2150A Kachina
Owner/operator:
Registration: N5601G
MSN: VAC189-85
Year of manufacture:1985
Engine model:Lycoming O-320
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Green Lake, WI -   United States of America
Phase: En route
Nature:Private
Departure airport:South Bend Regional, IN (SBN/KSBN)
Destination airport:Oshkosh-Wittman Field, WI (OSH/KOSH)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot reported that he was flying the airplane to the annual Experimental Aircraft Association Airventure fly-in at the Wittman Regional Airport (OSH), Oshkosh, Wisconsin, and was proceeding as prescribed in the Notices to Air Missions (NOTAM) pertaining to arrivals to the airport. He stated that the airplane's engine lost power and he activated the auxiliary fuel pump, which restored engine power briefly. The engine again lost power and the pilot executed a forced landing to a corn field. The airplane nosed over during the landing and incurred substantial damage to the fuselage and vertical tail.
Postaccident examination revealed no smell of fuel at the accident site and no evidence of a fuel spill. No usable quantity of fuel was found within the fuel tanks and the tanks were not breached. Examination of the airplane did not reveal any mechanical anomalies that would have precluded normal operation.
Automatic dependent surveillance - broadcast (ADS-B) data revealed that the flight lasted about 3.6 hours. According to the airplane operations manual, the maximum flight duration at normal cruise was about 3.9 hours without reserve, but was predicated on using a lean mixture setting.
Based on the available information, it is likely that the loss of engine power was due to fuel exhaustion.

Probable Cause: A loss of engine power due to fuel exhaustion, which resulted from the pilot's inadequate preflight planning.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CEN23LA329
Status: Investigation completed
Duration: 8 months
Download report: Final report

Sources:

NTSB CEN23LA329
FAA register: https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=5601G

https://flightaware.com/live/flight/N5601G/history/20230727/1355Z/KSBN/WI67

Location

Media:

Revision history:

Date/timeContributorUpdates
28-Jul-2023 14:43 hmmptwizzle Added
28-Jul-2023 14:45 harro Updated
28-Jul-2023 18:45 RobertMB Updated
29-Jul-2023 21:07 Captain Adam Updated
30-Jul-2023 08:30 Iceman 29 Updated
14-Aug-2023 20:43 Captain Adam Updated
28-Apr-2024 09:40 ASN Update Bot Updated [Time, Cn, Operator, Other fatalities, Source, Narrative, Category]

Corrections or additions? ... Edit this accident description

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