Accident Bell 206B-3 JetRanger III N5016G,
ASN logo
ASN Wikibase Occurrence # 33371
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Tuesday 4 August 1998
Time:08:45 LT
Type:Silhouette image of generic B06 model; specific model in this crash may look slightly different    
Bell 206B-3 JetRanger III
Owner/operator:Rainbow Helicopters
Registration: N5016G
MSN: 2624
Year of manufacture:1979
Total airframe hrs:5788 hours
Engine model:Allison 250-C20B
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Lucerne Valley, California -   United States of America
Phase: En route
Nature:Ferry/positioning
Departure airport:Riverside, CA (KRAL)
Destination airport:Flagstaff, AZ (KFLG)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot had been flying for about 25 minutes when he noticed that the oil pressure gauge and torque gauge were fluctuating. He initiated an approach to a precautionary landing spot on an asphalt pad. About 150 feet agl, the engine quit and the pilot autorotated to touch down on a paved road. The main rotor blades severed the tail boom aft of the horizontal stabilizer. The engine had received some maintenance work and had been reinstalled in the helicopter the night before the accident, at which time the pilot performed a test run and leak check of the engine, with no noted discrepancies. The pilot further stated that the engine had been running normally until the fluctuation of the oil pressure and torque gauges. During an examination of the engine, the oil output line was connected, but loose, and oil was seen dripping from the fitting area. Oil was observed over most of the fuselage and underneath the engine. There was approximately 1 pint of oil found in the sump. Further teardown of the engine revealed that the number 8 bearing was destroyed and no oil was found throughout the lubrication system. The Bell Helicopter maintenance manual specifies a torque value for the fitting on the oil output line; however, the mechanic who installed the engine reported that he did not use a torque wrench to tighten the line because he would have had to remove some other lines to get to it and he was in a hurry.

Probable Cause: The failure of the mechanic who installed the engine to follow proper procedures by insuring the proper torque to the oil output line, resulting in a loose fitting, oil loss and subsequent bearing failure.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX98LA256
Status: Investigation completed
Duration: 1 year and 7 months
Download report: Final report

Sources:

NTSB LAX98LA256
FAA register: 2. FAA: http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=5016G

Location

Revision history:

Date/timeContributorUpdates
27-Sep-2008 01:00 ASN archive Added
08-Apr-2015 20:20 Dr. John Smith Updated [Time, Operator, Total fatalities, Total occupants, Other fatalities, Location, Country, Phase, Nature, Departure airport, Destination airport, Source, Damage, Narrative]
08-Apr-2015 20:28 Dr. John Smith Updated [Narrative]
06-Apr-2024 17:04 ASN Update Bot Updated [Time, Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Damage, Narrative, Category, Accident report]

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org