Accident Schleicher ASH 26E N50FU,
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ASN Wikibase Occurrence # 345102
 
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Date:Thursday 31 August 2023
Time:13:39
Type:Silhouette image of generic AS26 model; specific model in this crash may look slightly different    
Schleicher ASH 26E
Owner/operator:Private
Registration: N50FU
MSN: 26248
Year of manufacture:2007
Fatalities:Fatalities: 1 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:near Wellington, CO -   United States of America
Phase: Manoeuvring (airshow, firefighting, ag.ops.)
Nature:Private
Departure airport:Owl Canyon Gliderport, CO (4CO2)
Destination airport:Wellington, CO
Investigating agency: NTSB
Confidence Rating: Information verified through data from accident investigation authorities
Narrative:
On August 31, 2023, about 1339 mountain daylight time, a Schleicher Alexander Gmbh & Co ASH 26E motor glider, N50FU, was substantially damaged when it was involved in an accident near Wellington, Colorado. The pilot sustained fatal injuries. The motor glider was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

Transmitted flight track data from the International Gliding Commission (IGC) flight recorder showed the self-launching motor glider depart to the northwest from the Owl Canyon Gliderport (4CO2) at 1320.

During the climb, several turns were performed and a maximum global positioning system (GPS) altitude of about 7,800 ft was observed at 1330. The IGC data showed the motor glider entered a steady descent on a northwest track, performed a 180° turn, and tracked to the southwest for about 2 miles before it turned back to the west. The IGC position at 1339:43 showed the motor glider on a track of about 296°, 60 knot groundspeed, and a GPS altitude 5,948 ft, which is about 250 ft above ground level.

The accident site was in a relatively flat agricultural field about 6 nautical miles northwest of the gliderport. The motor glider impacted the ground about 77° nose down attitude on a heading of 213° about 900 ft north of the last recorded position. The impact site consisted of a small circular depression and two ground scars that extended the length of the wingspan. The wreckage was located about 15 ft northeast of the impact site upright and oriented with the ground scar.

Flight control continuity from the motor glider control surfaces to the cockpit controls were confirmed. Both flap control surfaces, aileron control surfaces, and the cockpit flap actuator were in the landing position. Both wing airbrake surfaces were in the retracted position.

The propeller and driveshaft were in the “halfway in” position with no damaged observed to the propeller blades. The propeller was perpendicular to the storage position and the propeller stop control was in the non-stop position.

The wreckage was retained for further examination.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CEN23FA391
Status: Preliminary report
Duration:
Download report: Preliminary report

Sources:

https://kdvr.com/news/colorado/glider-aircraft-crash-in-larimer-county/
https://www.cbsnews.com/colorado/news/1-killed-glider-crashes-larimer-county/

NTSB
https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=50FU

Location

Media:

Revision history:

Date/timeContributorUpdates
01-Sep-2023 00:08 Captain Adam Added
01-Sep-2023 05:16 jw Updated
01-Sep-2023 05:16 RobertMB Updated
02-Sep-2023 17:18 Fibonacci Updated
05-Sep-2023 10:46 Captain Adam Updated

Corrections or additions? ... Edit this accident description

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