Accident Lancair IV N994PT,
ASN logo
ASN Wikibase Occurrence # 345528
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Saturday 25 December 2021
Time:09:25 LT
Type:Silhouette image of generic LNC4 model; specific model in this crash may look slightly different    
Lancair IV
Owner/operator:private
Registration: N994PT
MSN: LIV-407
Year of manufacture:2016
Total airframe hrs:599 hours
Engine model:Honeywell T-53-17A
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Iron Mountain, Michigan -   United States of America
Phase: Initial climb
Nature:Private
Departure airport:Iron Mountain, MI
Destination airport:Daytona Beach, FL (7FL6)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot reported that he took off at a reduced winter takeoff power setting. Once airborne and established on a climb, he retracted the landing gear and flaps, added climb power in increments, and then noticed a failure displayed on the generator control unit annunciator. About the same time, the pilot noticed the engine was quieter and the airspeed was decreasing. Onboard data indicated that, upon reaching 650 ft above ground level, about 50 seconds after the takeoff roll was initiated, the engine power reduced to idle with a simultaneous decrease in fuel flow. Several seconds later, a generator control unit failure warning illuminated, and the voltage began to slowly decrease, consistent with the generator turning off. The airplane continued to descend straight ahead and impacted trees and terrain about one nautical mile from the departure end of the runway. Both wings, the empennage, and the engine separated from the fuselage.

Following the accident, the condition lever was in an aft position. The pilot stated that, due to the altitude at the time he identified the loss of engine power, he did not take any actions to feather the propeller or restart the engine. A postaccident examination of the engine and related systems revealed no evidence of any preimpact mechanical malfunctions or failures that would have precluded normal operation. The recorded engine data is consistent with a reduction in commanded engine power and ultimately an in-flight shutdown. While it is possible that the condition lever came back with the flap activation and was not noted by the pilot, investigators were not able to determine when or how the condition lever was moved aft.

Probable Cause: The total loss of engine power after takeoff for undetermined reasons.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CEN22LA089
Status: Investigation completed
Duration: 1 year and 8 months
Download report: Final report

Sources:

NTSB CEN22LA089

Location

Revision history:

Date/timeContributorUpdates
14-Sep-2023 10:26 ASN Update Bot Added
14-Sep-2023 19:26 harro Updated

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org