Accident Smyth Sidewinder N86S,
ASN logo
ASN Wikibase Occurrence # 34801
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Monday 8 January 1996
Time:17:57 LT
Type:Smyth Sidewinder
Owner/operator:Private
Registration: N86S
MSN: 212090
Total airframe hrs:500 hours
Engine model:Lycoming O-320-B2B
Fatalities:Fatalities: 1 / Occupants: 1
Aircraft damage: Destroyed
Category:Accident
Location:Oklahoma City, OK -   United States of America
Phase: En route
Nature:Private
Departure airport:(KHSD)
Destination airport:Tulsa, OK (KTUL)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot had just purchased the airplane and was planning to return to his home in Tulsa, Oklahoma. He and the seller flew the airplane on an 'orientation ride' for 'approximately 10 minutes' before the pilot departed. According to the seller, the pilot had considerable experience in a similar airplane, but the fuel selector handles in the two airplanes were configured in an opposite manner. The accident airplane was observed to depart from runway 17 and turn east. At approximately a quarter of a mile from the airpark and at approximately 500 feet AGL, the engine began to 'sputter.' About 8 seconds later, the engine 'quit.' The airplane continued east and was observed to make a gentle bank to the right and then to the left, but 'the nose was never lowered to establish a glide.' The airplane was observed to stall and spin to the left, rotating about 2 turns before impacting the ground. Postimpact examination of the fuel selector handle and valve revealed they were in the 'off' position.

Probable Cause: The pilot's improper positioning of the fuel selector, which resulted in fuel starvation and loss of engine power, and his failure to maintain sufficient airspeed while coping with the emergency, which resulted in and inadvertent stall and subsequent spin. Factors relating to the accident were: the pilot's lack of experience in type of airplane, and habit interference with respect to use of the fuel selector.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: FTW96FA085
Status: Investigation completed
Duration: 7 months
Download report: Final report

Sources:

NTSB FTW96FA085

Location

Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
09-Apr-2024 08:43 ASN Update Bot Updated [Time, Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative, Category, Accident report]

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org