ASN Wikibase Occurrence # 35162
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Date: | Monday 18 January 1993 |
Time: | 18:29 |
Type: | Beechcraft V35B Bonanza |
Owner/operator: | Midwest Aviation |
Registration: | N74DC |
MSN: | D-9610 |
Total airframe hrs: | 1721 hours |
Fatalities: | Fatalities: 3 / Occupants: 3 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Dixie Inn, LA -
United States of America
|
Phase: | Approach |
Nature: | Executive |
Departure airport: | Paducah, KY (PAH) |
Destination airport: | Shreveport, LA (SHV) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE MODE C READOUT HAD BEEN INTERMITTENT DURING THE FLIGHT; HOWEVER, THE PILOT DID NOT REPORT ANY PROBLEMS WITH THE FLIGHT INSTRUMENTS OR AIRCRAFT SYSTEMS. UPON ARRIVAL IN THE DESTINATION AREA, THE PILOT WAS ISSUED RADAR VECTORS AND INSTRUCTED TO INITIATE A DESCENT FROM 6,000 TO 3,000 FEET. THE INITIAL STAGE OF THE DESCENT APPEARED NORMAL ON RADAR. HOWEVER, UPON REACHING 5,100 FEET, THE TARGET WENT INTO THE COAST MODE AND RADAR AND RADIO CONTACT WAS LOST. THE WRECKAGE WAS FOUND 2 DAYS LATER, SPREAD OUT OVER 200 FEET THROUGH DENSE WOODS ABOUT 2.5 MILES ALONG THE ROUTE OF FLIGHT FROM THE POINT OF LAST RADAR CONTACT. INVESTIGATION DID NOT REVEAL ANY EVIDENCE OF AIRFRAME, ENGINE OR SYSTEMS FAILURE AND THERE WAS NO EVIDENCE THAT ICING CONDITIONS EXISTED DURING THE DESCENT PHASE OF THE FLIGHT. CAUSE: THE PILOT'S FAILURE TO MAINTAIN CONTROL FOR UNDETERMINED REASONS.
Sources:
NTSB:
https://www.ntsb.gov/ntsb/brief.asp?ev_id=20001211X11691 Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
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