Serious incident Piper PA-42-1000 N37KW,
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ASN Wikibase Occurrence # 351877
 
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Date:Friday 5 February 1999
Time:11:00 LT
Type:Silhouette image of generic PAY4 model; specific model in this crash may look slightly different    
Piper PA-42-1000
Owner/operator:Cumberland Mangement
Registration: N37KW
MSN: 425527039
Year of manufacture:1989
Total airframe hrs:3694 hours
Engine model:Garrett TPE-331-14
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Minor
Category:Serious incident
Location:near Lexington, Kentucky -   United States of America
Phase: En route
Nature:Private
Departure airport:Wilmington-New Castle County Airport, DE (KILG)
Destination airport:Lexington-Blue Grass Airport, KY (LEX)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The during descent for landing, the airplane's right engine, a TPE331-14B, experienced an uncontained gearcase failure. Disassembly of the engine revealed that the gearcase was ruptured in the 1st bull gear's plane of rotation and that the 1st bull gear had a 90 degree arc of the rim and gear teeth separated. Metallurgical examination of the 1st bull gear revealed a fatigue fracture that had originated in the gear's bore splines.
The fatigue originated in area where the spline thickness was significantly reduced by indentations on the pressure surface of the splines. Review of the engine's overhaul manual revealed a tie-rod was used to provide a clamping force between the spur gear and 1st bull gear. The assembly procedures required that the tie-rod be stretched with a load of 22,000 pounds, and then secured with a nut that was hand-tightened. During disassembly of the gearcase, it was not possible to determine the amount of stretch on the tie-rod, or the breakaway torque on the retaining nut. Maintenance records revealed that the gearcase was disassembled, and reassembled during repairs, which were performed by engine manufacturer.

Probable Cause: Improper assembly of the engine gearcase by the manufacturer, which resulted in an uncontained failure of the 1st bull gear.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: NYC99IA056
Status: Investigation completed
Duration: 1 year and 9 months
Download report: Final report

Sources:

NTSB NYC99IA056

Revision history:

Date/timeContributorUpdates
21-Feb-2024 20:48 ASN Update Bot Added
21-Feb-2024 20:52 ASN Updated [Aircraft type, Operator, Location, Phase, Departure airport, Destination airport, Narrative]

Corrections or additions? ... Edit this accident description

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