Fuel exhaustion Accident Glasair III N153JC,
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ASN Wikibase Occurrence # 352545
 
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Date:Thursday 23 September 1999
Time:19:00 LT
Type:Silhouette image of generic GLAS model; specific model in this crash may look slightly different    
Glasair III
Owner/operator:private
Registration: N153JC
MSN: 3236
Total airframe hrs:58 hours
Engine model:Lycoming IO-540
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Snelling, CA -   United States of America
Phase: En route
Nature:Private
Departure airport:Minden, NV (KMEV)
Destination airport:San Luis Obispo, CA (SLO
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
About 25 minutes into the flight over mountainous terrain, the pilot noticed that the left fuel cap was missing, and that fuel was escaping from the left tank filler opening. The pilot said he selected the right tank, but then returned the selector to the both position. He descended to make a precautionary landing at an airport ahead of the airplane and the engine quit during the en route descent. He landed in a field with the landing gear retracted and impacted a fence. An FAA inspector examined the airplane during recovery operations. As it was being lifted, he observed about 1 quart of fuel drain from the left wing tank. When the selector was positioned to both about 1 gallon drained from the belly in a continuous stream. According to the pilot and a mechanic who worked on the airplane before the flight, while at the departure airport the pilot had several electrical system problems that required several days to repair. During this time as electrical components were being replaced, engine starts became problematic. The mechanic pressurized the fuel tank with air through the left tank fuel filler opening and the engine started without difficulty. The mechanic suspected that the electric fuel pump was the cause of the problem and advised the pilot to have the pump examined. The pilot decided to continue with his flight plans instead. The pilot stated that he did not do his own preflight check of the airplane; he assumed that the fuel cap had been replaced. The mechanic reported that the pilot replaced the cowling and restarted the engine. Three witnesses watched the airplane taxi out and depart. No fuel caps were found on the ramp or the runway.

Probable Cause: The pilot's inadequate preflight inspection, which failed to ensure that the left fuel filler cap was secure, and his decision to continue flight with a known malfunction in the electric fuel pump. Also causal was the pilot's improper positioning of the fuel selector to the both selection after the siphoning fuel condition was noted from the left tank filler opening, which resulted in fuel exhaustion.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX99LA318
Status: Investigation completed
Duration: 1 year and 6 months
Download report: Final report

Sources:

NTSB LAX99LA318

History of this aircraft

Other occurrences involving this aircraft
11 October 1997 N153JC Private 0 Desert Center, CA sub

Location

Revision history:

Date/timeContributorUpdates
08-Mar-2024 08:01 ASN Update Bot Added

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