ASN Wikibase Occurrence # 352827
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Date: | Thursday 12 August 1999 |
Time: | 12:34 LT |
Type: | Lancair IV-P |
Owner/operator: | Private |
Registration: | N124KM |
MSN: | 141 |
Total airframe hrs: | 550 hours |
Engine model: | Continental TSIO-550-B1B |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Aspen, CO -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Goodland, KS (KGLD) |
Destination airport: | (KASE) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During the pilot's second landing attempt, the aircraft touched down near taxiway A2, 1,800 feet down the 7,004 foot runway. The airplane then failed to stop, and departed the end of the runway slightly left of the centerline into a grassy, rocky ditch. The pilot stated that after allowing the nose wheel to settle onto the runway, he applied brake pressure and the right brake appeared soft. He was not able to initiate a go-around due to the high density altitude (calculated to be 9,828 ft. mean sea level), and limited remaining runway. According to a mechanic employed at the airport, he observed a red fluid running down the right gear strut following the accident. A functional brake test of the right brake was performed, and it was confirmed that the right brake was 'soft.' The wind at the time the pilot landed was from 300 degrees at 10 knots. The airport normally directs traffic to land on runway 15 due to mountainous terrain, despite existing wind conditions.
Probable Cause: A failure of the right landing gear's brake system. Factors were the improper touchdown point attained by the pilot, the existing weather conditions that included a tailwind and high density altitude, and the rocky ditch.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | DEN99LA144 |
Status: | Investigation completed |
Duration: | 1 year and 2 months |
Download report: | Final report |
|
Sources:
NTSB DEN99LA144
Location
Revision history:
Date/time | Contributor | Updates |
08-Mar-2024 20:31 |
ASN Update Bot |
Added |
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