ASN Wikibase Occurrence # 352848
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Date: | Tuesday 10 August 1999 |
Time: | 17:30 LT |
Type: | Beechcraft H-35 |
Owner/operator: | Private |
Registration: | N7975D |
MSN: | D5265 |
Total airframe hrs: | 5360 hours |
Engine model: | Continental O-470G |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Swan Lake, MT -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Creston, MT |
Destination airport: | Benchmark, MT (3U7 |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot observed a rpm overspeed with oil temperature rise. Throttling back relieved the overspeed situation; however, he observed a rapid loss of remaining power after turning back toward a potential emergency landing airstrip. He stated that the propeller had continued windmilling until impact. Pistons 1, 2, 4, 5, and 6 had few combustion deposits on their combustion faces. Piston 3 exhibited evidence of detonation, including a hole of about 1 inch diameter, and a combustion surface with the appearance of erosion. As originally manufactured, minimum octane requirement for this engine fuel was 91/96 octane. Teledyne Continental Motors amended the recommended fuel to 100 octane after 91/96 octane fuel became obsolete. Placards on the airplane fuel tanks stated that minimum fuel required was 100 octane. No evidence was found of a Supplemental Type Certificate for use of automotive gasoline in the subject airplane or engine. A sample of the automotive fuel removed from the airplane after the accident was tested: Research Octane Number was 94, Motor Octane Number was 83.8, and anti-knock index was 88.9. The pilot stated that he had been using automotive gasoline in the airplane for approximately 700 hours.
Probable Cause: Detonation/pre-ignition due to use of improper grade and type of fuel (automotive) and the pilot-in-command's failure to use proper fuel specified by manufacturer's directives.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | SEA99FA138 |
Status: | Investigation completed |
Duration: | 1 year and 3 months |
Download report: | Final report |
|
Sources:
NTSB SEA99FA138
Location
Revision history:
Date/time | Contributor | Updates |
09-Mar-2024 06:44 |
ASN Update Bot |
Added |
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