Accident Bell 47G-3B-1 Soloy N4002G,
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ASN Wikibase Occurrence # 353003
 
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Date:Saturday 17 July 1999
Time:16:30 LT
Type:Bell 47G-3B-1 Soloy
Owner/operator:Precision Air Services, Inc.
Registration: N4002G
MSN: 6529
Year of manufacture:1966
Total airframe hrs:10013 hours
Engine model:Allison T63-A700
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Sour Lake, TX -   United States of America
Phase: Initial climb
Nature:Agricultural
Departure airport:
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The helicopter lost engine power during takeoff due to contaminated fuel. The commercial helicopter pilot stated that the night before the accident flight, the fueling truck, which contained three tanks (one each for water, chemicals, and fuel), was checked. The pilot stated that the fuel appeared 'normal' that night. The following day, prior to the accident flight, the helicopter was 'refueled without sumping the tanks.' The pilot added that during takeoff, the engine lost power about 50 feet above the ground, at 30 miles per hour. He executed an autorotation to the ground where the main rotor blades impacted the tail boom and the tail rotor blades contacted the ground. The pilot stated that he found 20 gallons of water in the helicopter's fuel tank after the accident. He added that he discovered the fuel truck had a crack in between the water and fuel tanks. Approximately 80 gallons of water had leaked into the truck's fuel tank. The fuel truck was 'supposed to have an aqua stop filter installed that will not pump if water is present but the wrong filter was installed.'

Probable Cause: The pilot's failure to adequately preflight the helicopter's fuel system resulting in the total loss of engine power as a result of water contamination. Factors were the incorrect filter installed on the fueling truck and the pilot's improper touchdown technique.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: FTW99TA194
Status: Investigation completed
Duration: 1 year and 4 months
Download report: Final report

Sources:

NTSB FTW99TA194

History of this aircraft

Other occurrences involving this aircraft
19 October 2002 N4002G Holcomb Aerial Service Inc 0 Highfalls, Georgia sub
Fuel exhaustion
3 August 2015 N4002G Ewing Flying Service Llc 0 Camden, AL sub

Location

Revision history:

Date/timeContributorUpdates
09-Mar-2024 09:21 ASN Update Bot Added

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