ASN Wikibase Occurrence # 353098
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Date: | Thursday 1 July 1999 |
Time: | 20:40 LT |
Type: | Piper PA-24-260 |
Owner/operator: | Private |
Registration: | N5788 |
MSN: | 24-4580 |
Year of manufacture: | 1966 |
Total airframe hrs: | 4775 hours |
Engine model: | Lycoming IO-540D |
Fatalities: | Fatalities: 0 / Occupants: 4 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Houston, TX -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | New Braunfels, TX |
Destination airport: | (KIWS) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot failed to maintain the proper descent rate during a VFR approach, in dusk light conditions, following a complete loss of engine power, and the airplane undershot the runway. The airplane was on the downwind leg at 1,100 feet agl and was abeam the runway numbers when the pilot extended the landing gear. Simultaneously, she heard a loud bang and noticed a loss of engine power. The pilot advanced the throttle and realized that the engine had lost total power. The pilot stated that she trimmed the airplane to attain the best glide speed, but did not verify the airspeed during the ensuing forced landing. She added that the airplane was descending 'too fast,' and she needed 'more trim to relieve back pressure, but decided to muscle it as best [she] could and try not to stall the airplane.' Subsequently, the airplane's nose wheel contacted a cement drainage ditch at the approach end of the runway. Following the accident, the engine was test run in the airframe and found to operate within the manufacturer's specifications.
Probable Cause: The pilot's failure to maintain the proper descent rate during a forced landing, which resulted in a runway undershoot. Factors were the total loss of engine power for an undetermined reason and the dusk light conditions.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW99LA178 |
Status: | Investigation completed |
Duration: | 11 months |
Download report: | Final report |
|
Sources:
NTSB FTW99LA178
Location
Revision history:
Date/time | Contributor | Updates |
09-Mar-2024 10:22 |
ASN Update Bot |
Added |
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