ASN Wikibase Occurrence # 353173
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Date: | Tuesday 15 June 1999 |
Time: | 10:04 LT |
Type: | Velocity XL/RG |
Owner/operator: | Private |
Registration: | N19DW |
MSN: | 3RX026 |
Total airframe hrs: | 117 hours |
Engine model: | Lycoming IO-540-E4C5 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Fort Pierce, FL -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Hollywood, FL (HWO |
Destination airport: | Fort Pierce, FL |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:While maneuvering in cruise flight, the pilot/builder of the experimental airplane noticed a fluctuating fuel pressure gage and then the engine quit. The pilot executed a forced landing onto an interstate highway. Postcrash examination revealed an empty right wing fuel tank and no other abnormality of the fuel system and engine. Postcrash start and operation of the engine was satisfactory. The pilot/builder revealed that ever since he changed fuel filler caps, two flights before the accident flight, he had experienced fuel tank imbalance problems. A factory test pilot, using wing tank caps of various tightness adjustments, revealed that gravity feed from wing tank to sump tank could be interrupted if the cap were allowed to fit loosely and allow siphoning due to upper wing surface low pressure while inflight. As a result of the testing, the factory has increased the size of the fuel vent plumbing, eliminated the sump tank vent in favor of an air bleed, 'burp valve', and sent out alerts to all kit owners about fuel starvation resulting from loose-fitting caps.
Probable Cause: The owner/pilot mechanic's failure to adjust the newly installed wing fuel caps resulting in the loss of engine power while in cruise flight due to fuel starvation and the subsequent collision with transmission wires while attempting a forced landing to a highway. Factors in the accident were the failure of the vent system to adequately compensate for the pressure differential created and the failure of the pilot to monitor fuel balance.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA99LA184 |
Status: | Investigation completed |
Duration: | 1 year and 8 months |
Download report: | Final report |
|
Sources:
NTSB MIA99LA184
Location
Revision history:
Date/time | Contributor | Updates |
09-Mar-2024 11:09 |
ASN Update Bot |
Added |
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