Accident Boeing 757-232 N656DL,
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Date:Wednesday 2 June 1999
Time:20:26 LT
Type:Silhouette image of generic B752 model; specific model in this crash may look slightly different    
Boeing 757-232
Owner/operator:Delta Air Lines
Registration: N656DL
MSN: 24396/266
Year of manufacture:1990
Total airframe hrs:32549 hours
Engine model:P&W PW2037
Fatalities:Fatalities: 0 / Occupants: 127
Aircraft damage: Substantial
Category:Accident
Location:Phoenix-Sky Harbor International Airport, AZ (PHX/KPHX) -   United States of America
Phase: Landing
Nature:Passenger - Scheduled
Departure airport:New York, NY (KJFK)
Destination airport:Phoenix-Sky Harbor International Airport, AZ (PHX/KPHX)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The airplane sustained substantial structural damage to the nose wheel well aft bulkhead during a hard landing. The en route flight from New York to Phoenix was uneventful. About 3 seconds before touchdown, at the termination of a visual approach, the airplane's pitch attitude increased to 5.8 degrees. The captain, who was the flying pilot, described the first touchdown as being 'firm,' and in the runway's touchdown zone, close to the centerline. There was a maintenance carry over (MCO) disabling the auto-spoiler deployment system, so the first officer manually deployed the spoilers upon touchdown. The captain stated he then applied forward pressure to the control yoke. The captain additionally reported that he 'felt a jolt' as the nose gear returned to the runway. After landing, the airplane taxied to the gate. It was subsequently examined and substantial damage was observed to the airplane's nose gear wheel well aft bulkhead, associated underlying structure, and skin panels. The digital flight data recorder was read out and it revealed that approximately 3 seconds prior to touchdown, the pitch attitude started increasing in response to nose up elevator inputs to a maximum pitch of about 5.8 degrees, and the airplane touched down (transitioned from air to ground) then became airborne again. The second air to ground transition occurred 3 seconds later and the elevator positions changed over the next second from plus 6 degrees to minus 16 degrees as the pitch attitude rapidly decreased to -0.7 degrees at a rate of 4 degrees per second. There was no evidence of any mechanical malfunctions during the landing event.

Probable Cause: The pilot's excessive and rapid forward control column movement in response to a bounced landing, which resulted in the hard touchdown of the nose wheel.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX99FA207
Status: Investigation completed
Duration: 1 year and 12 months
Download report: Final report

Sources:

NTSB LAX99FA207

Location

Revision history:

Date/timeContributorUpdates
09-Mar-2024 11:56 ASN Update Bot Added

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