Accident Cessna 180 N9270C,
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ASN Wikibase Occurrence # 353270
 
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Date:Friday 28 May 1999
Time:13:40 LT
Type:Silhouette image of generic C180 model; specific model in this crash may look slightly different    
Cessna 180
Owner/operator:Private
Registration: N9270C
MSN: 31369
Year of manufacture:1955
Total airframe hrs:2700 hours
Engine model:Continental O-470K
Fatalities:Fatalities: 0 / Occupants: 3
Aircraft damage: Substantial
Category:Accident
Location:Sedona, AZ -   United States of America
Phase: Approach
Nature:Private
Departure airport:Wichita, KS (KICT)
Destination airport:(KSEZ)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot and two passengers departed Wichita, Kansas, for a planned nonstop flight to Sedona, Arizona. The pilot was familiar with the route and had about 1,800 hours flying experience in the airplane, which had been modified to hold 73 gallons of fuel. While en route, all airplane systems functioned normally, and no adverse weather was encountered. Fuel exhaustion occurred upon arrival over the destination airport at 8,500 feet msl. The pilot repositioned the fuel selector to the left fuel tank, but engine power was not restored. The airport's elevation is 4,827 feet msl, and the runway is 5,132 feet long. The pilot descended into the airport's downwind leg, and then turned onto the base leg and final approach leg for runway 21. He reported experiencing a 15- to 20-knot wind from 270 degrees. Unable to glide to the runway, the pilot touched down hard in the dirt between 10 and 15 feet short of the runway, in a stalled attitude. The left main wheel contacted an 8- to 10-inch asphalt berm at the approach end of the runway. After the accident the pilot attempted to start the engine. He stated that the left fuel tank contained several gallons of fuel, and after several seconds of cranking the engine started and operated normally. He also reported that during the flight all of the airplane's systems had functioned normally. Under the direction of the Safety Board, an airframe and powerplant mechanic examined the airplane. The mechanic reported that both of the airplane's wing fuel tank gauges and the auxiliary tank gauge registered empty.

Probable Cause: Fuel exhaustion due to an inadequate fuel supply, and the pilot's inadequate in-flight planning fuel consumption calculations.

Accident investigation:
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Investigating agency: NTSB
Report number: LAX99LA205
Status: Investigation completed
Duration: 1 year and 5 months
Download report: Final report

Sources:

NTSB LAX99LA205

Location

Revision history:

Date/timeContributorUpdates
09-Mar-2024 12:09 ASN Update Bot Added

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