ASN Wikibase Occurrence # 353417
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Date: | Monday 26 April 1999 |
Time: | 09:30 LT |
Type: | Cessna 206H |
Owner/operator: | Palwaukee Aviation |
Registration: | N42122 |
MSN: | 25 |
Total airframe hrs: | 11 hours |
Engine model: | Lycoming IO-540 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | None |
Category: | Serious incident |
Location: | Wheeling, IL -
United States of America
|
Phase: | Standing |
Nature: | Ferry/positioning |
Departure airport: | |
Destination airport: | Naperville, IL (LL10) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During the run-up flight control checks prior to takeoff, the pilot experienced an aileron control failure. He was unable to obtain left aileron up movement. Inspection determined that the aileron had 4 degrees of up travel. Normal travel was 20 degrees /- 2 degrees. Further inspection revealed that one of the aileron control bellcrank stop bolt/jam nut assemblies was loose allowing the stop bolt to rotate out of the threaded boss. This restricted the aileron movement. The three other stop bolt/jam nut assemblies were also inspected and were found to be loose. The airplane was a 1999 model, s/n 25, which had a total of approximately 11 hours on it at the time of the incident. In response to this incident Cessna Aircraft Company issued Special Service Project SSP99-27-02. On June 21, 1999, the Federal Aviation Administration issued Airworthiness Directive, 99-13-04, effective July 13, 1999. The AD requires '...inspecting the left and right wing aileron control bellcrank stop bolts and lock nuts for flush and tight contact with the surface of the threaded boss on each end of the yoke assemblies, and accomplishing follow-on and corrective actions, as applicable.'
Probable Cause: improper installation of the aileron control bellcrank stop bolts and lock nuts during the manufacturing process which resulted in a binding aileron control surface.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI99IA144 |
Status: | Investigation completed |
Duration: | 2 years and 3 months |
Download report: | Final report |
|
Sources:
NTSB CHI99IA144
Location
Revision history:
Date/time | Contributor | Updates |
09-Mar-2024 13:47 |
ASN Update Bot |
Added |
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