ASN Wikibase Occurrence # 353428
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 13 March 1999 |
Time: | 16:00 LT |
Type: | Gulfstream G-IV |
Owner/operator: | Zeno Air Inc. |
Registration: | N411WW |
MSN: | 1121 |
Year of manufacture: | 1989 |
Total airframe hrs: | 5196 hours |
Engine model: | Rolls-Royce TAY 611-8 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Minor |
Category: | Serious incident |
Location: | Durango, CO -
United States of America
|
Phase: | En route |
Nature: | Ferry/positioning |
Departure airport: | Santa Barbara, CA |
Destination airport: | Chicago-Midway Airport, IL (MDW/KMDW) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane was cruising at 41,000 feet msl when the crew noticed low fuel flow and low EGT readings on the left engine. They further noted that the oil temperature and fuel temperature gauges began to rise on the same engine. They requested clearance to descend, and as the captain reduced the throttle, the fire light on the left engine illuminated. He pulled the left fire T-handle and the fire light extinguished. The crew secured the engine, requested emergency equipment be standing by in Durango, and landed without further incidence. Postaccident examination revealed that the lower forward area of the left engine nacelle was damaged by fire. Further examination revealed that an electrical wire coming from an alternator in the engine had been chaffing against the number four fuel line.
Probable Cause: The failure of the number four fuel line. Factors were the chaffing of the alternator's electrical wires on the number four fuel line, and the subsequent fire in the number one engine nacelle.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | DEN99IA053 |
Status: | Investigation completed |
Duration: | 1 year and 3 months |
Download report: | Final report |
|
Sources:
NTSB DEN99IA053
History of this aircraft
Other occurrences involving this aircraft
1 January 2020 |
N962SS |
Executive Charters Inc |
0 |
Van Nuys, CA |
|
non |
Turbulence |
Location
Revision history:
Date/time | Contributor | Updates |
09-Mar-2024 13:53 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation