Accident Mooney M20J N201QK,
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ASN Wikibase Occurrence # 353566
 
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Date:Monday 16 November 1998
Time:20:45 LT
Type:Silhouette image of generic M20P model; specific model in this crash may look slightly different    
Mooney M20J
Owner/operator:Private
Registration: N201QK
MSN: 24-0290
Total airframe hrs:3932 hours
Engine model:Lycoming IO-360-A1B6D
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:San Angelo, TX -   United States of America
Phase: En route
Nature:Private
Departure airport:Levelland, TX (Q24)
Destination airport:(KSJT)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The airplane was en route cruising at 9,500 feet msl approximately 12 miles east of its destination, when the pilot reported a loss of engine power. At 2,200 feet msl, the pilot reported that he would not make the runway. During the off airport landing, the airplane struck a tree, the right wing separated from the airframe, the airplane descended into the water, and came to rest inverted in water 7 feet deep. Examination of the wreckage revealed engine oil in the single drive dual magneto and one of the rear case bearing retaining plate screws was broken. The magneto was removed from the engine and disassembled. A metallurgist found that screw failure was a result of delayed fracture from hydrogen embrittlement and the 'hydrogen was most likely picked up during the cadmium plating for corrosion resistance at original manufacture of the screw.' The magneto had accumulated 775.58 hours since last overhaul in 1993. At the last annual inspection, November 1998, the magneto points and timing were checked. Time since that annual inspection was 3.27 hours. Service Bulletin (SB) 643 dated 02/08/94 recommended magnetos be 'overhauled or replaced at the expiration of four years without regard to the accumulated operating hours since new or last overhaul.' No evidence was found that the SB had been accomplished; however, under 14 CFR Part 91 operations, compliance with the SB is not required.

Probable Cause: The total loss of engine power due to the magneto failure resulting from oil contamination when the bearing plate retainer screw fractured due to improper manufacturing. Factors were the lack of suitable terrain for the forced landing, and the dark night conditions.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: FTW99LA027
Status: Investigation completed
Duration: 10 months
Download report: Final report

Sources:

NTSB FTW99LA027

Location

Revision history:

Date/timeContributorUpdates
10-Mar-2024 08:09 ASN Update Bot Added

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