ASN Wikibase Occurrence # 353594
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Date: | Friday 6 November 1998 |
Time: | 23:11 LT |
Type: | Cessna 172N |
Owner/operator: | Dolphin Holiday Flying Club |
Registration: | N1901S |
MSN: | 17267660 |
Total airframe hrs: | 3961 hours |
Engine model: | Lycoming O-320-H2AD |
Fatalities: | Fatalities: 0 / Occupants: 4 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Fort Lauderdale, FL -
United States of America
|
Phase: | Initial climb |
Nature: | Training |
Departure airport: | (KFXE) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The flight departed, performed airwork, then executed a practice ILS approach to the runway. After touchdown about 2,000 feet down the 6,001 foot long runway with the flaps fully extended, the pilot-rated student performed a touch-and-go landing and placed the flap selector to the 'up' position. The flight continued and climbed to about 100 feet where while flying near the departure end of the runway, the CFI noted that the airspeed was not increasing. One of the rear seat occupants advised him that the flaps failed to retract and unable to maintain altitude, the CFI maneuvered the airplane for a forced landing on a road. While flaring for landing, the left elevator contacted the roof of a vehicle. The airplane then touched down, collided with a light pole, and came to rest upright. Post accident examination of the airplane revealed that the flap circuit breaker was popped; no determination could be made as to the reason for flap malfunction. The flaps were determined to be fully extended and the airplane was about 39 pounds over gross weight at the time of the accident.
Probable Cause: The failure of the pilot-in-command to note that the flaps did not retract while the pilot-rated student performed a touch-and-go landing on a 6,001 foot-long runway. Factors in the accident were the total failure of the flap system for undetermined reasons and the operation of the airplane in an overgross weight condition by the pilot-in-command (CFI).
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA99LA030 |
Status: | Investigation completed |
Duration: | 2 years and 3 months |
Download report: | Final report |
|
Sources:
NTSB MIA99LA030
Location
Revision history:
Date/time | Contributor | Updates |
10-Mar-2024 08:28 |
ASN Update Bot |
Added |
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