ASN Wikibase Occurrence # 353777
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Date: | Friday 18 September 1998 |
Time: | 09:31 LT |
Type: | Piper PA-44-180 |
Owner/operator: | Discovery Aviation Services |
Registration: | N39776 |
MSN: | 44-7995030 |
Year of manufacture: | 1978 |
Total airframe hrs: | 7235 hours |
Engine model: | Lycoming O-360-E1A6D |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Titusville, FL -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | (KTIX) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The landing gear hydraulic pump was replaced and reportedly checked satisfactory during annual inspection signed off 1 day earlier. The flight departed and after reportedly lowering the landing gear selector handle, the landing gear down and locked lights did not illuminate. The pilot cycled the navigation light switch, flew by the tower and was advised the gear appeared down and locked. He retracted the gear, reentered the traffic pattern, and again lowered the gear handle, but again, there were no down and locked lights from the landing gears nor a gear unsafe light. The pilot landed the airplane and reportedly after touchdown, the left main landing gear began to collapse. The airplane veered off the left side of the runway into grass and came to rest with the left and nose landing gears down and locked; the right main landing gear was collapsed. Post accident testing of the left main landing gear revealed no evidence of failure or malfunction; the down and locked light illuminated. The hydraulic pump was removed, bench tested, and found to operate normally. Testing of hydraulic fluid revealed it was contaminated beyond allowable limits. There was no requirement by the airplane manufacturer to replace the hydraulic fluid. The pilot reported that he did not utilize the emergency gear extension.
Probable Cause: The collapse of the right main landing gear for undetermined reasons. A contributing factor was the pilot's failure to execute the emergency gear extension procedure.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA98LA248 |
Status: | Investigation completed |
Duration: | 1 year and 6 months |
Download report: | Final report |
|
Sources:
NTSB MIA98LA248
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
10-Mar-2024 10:24 |
ASN Update Bot |
Added |
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