ASN Wikibase Occurrence # 353967
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Date: | Saturday 8 August 1998 |
Time: | 16:05 LT |
Type: | Bell 212 |
Owner/operator: | BLM, U.S. Dept Of Interior |
Registration: | N291B |
MSN: | 30842 |
Year of manufacture: | 1977 |
Total airframe hrs: | 11806 hours |
Engine model: | P&W PT6T-3 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Juntura, OR -
United States of America
|
Phase: | Taxi |
Nature: | Unknown |
Departure airport: | Burns, OR (KBNO) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot-in-command (PIC) had just maneuvered the Bell 212 helicopter into a 100 foot hover above a small reservoir to fill a 'Bambi' bucket for fire-fighting operations. The rotorcraft began to settle. The PIC, perceiving that he had encountered rotor vortex conditions, slipped the helicopter to the right with the bucket still in the reservoir. This, in turn, increased the angle of the long line from the vertical or zero degree reference. Immediately thereafter, the PIC noted a loss of power in the #1 engine. He then executed a single-engine autorotation, during which a rotor blade impacted a dead tree. Post-crash examination revealed that the long line had pulled aft and left from its vertical reference into the airframe structure (the 7:30 position of the hell hole in the belly of the helicopter) resulting in 1) the separation of one of the #1 engine push/pull rods, and 2) the deformation of engine control rods associated with the #1 engine flight idle stop (solenoid) which then sheared. The shearing of the flight idle stop resulted in a restriction/cessation of fuel flow to the #1 engine fuel control unit, and subsequent engine shutdown.
Probable Cause: The pilot-in-command's failure to maintain proper clearance between the long line cable and hell hole structure resulting in airframe contact and binding of the cable. This resulted in separation/disabling of the fuel control solenoid and a subsequent restriction/cessation of fuel flow to the #1 engine. Contributing factors were separation of the #1 engine push/pull rod and a tree.
Accident investigation:
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| |
Investigating agency: | NTSB |
Report number: | SEA98GA159 |
Status: | Investigation completed |
Duration: | 1 year and 5 months |
Download report: | Final report |
|
Sources:
NTSB SEA98GA159
History of this aircraft
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Location
Revision history:
Date/time | Contributor | Updates |
10-Mar-2024 17:30 |
ASN Update Bot |
Added |
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