ASN Wikibase Occurrence # 353978
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Date: | Friday 7 August 1998 |
Time: | 12:20 LT |
Type: | Cessna 150J |
Owner/operator: | Private |
Registration: | N60564 |
MSN: | 15070408 |
Total airframe hrs: | 4539 hours |
Engine model: | Continental O-200A |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Belen, NM -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | (E80) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot told FAA inspectors that he detected water in the fuel during his preflight, and thought he had drained all the water from the tanks. In his accident report, however, he made no reference to his preflight. Shortly after departing runway 21, the engine lost power but was 'surging'. The pilot tried to land on a road but was unable. The pilot stated the 'aircraft [was] in ground effect with [the] stall warning horn in operation.' He 'flew within 30 yards of road when [he] could no longer keep in ground effect with power that the engine was producing.' The pilot made a forced landing on soft sandy soil south of the airport. The aircraft rolled approximately 20 feet and nosed over. FAA inspectors reported draining a considerable quantity of 'rust red' water from both fuel tanks and debris from the gascolator, and the aircraft did not have a valid certificate of airworthiness or registration.
Probable Cause: The pilot's improper preflight in that he failed to drain the water from the fuel sumps. Factors were water contamination in the fuel tank and a sand bar.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW98LA357 |
Status: | Investigation completed |
Duration: | 2 years and 6 months |
Download report: | Final report |
|
Sources:
NTSB FTW98LA357
Location
Revision history:
Date/time | Contributor | Updates |
10-Mar-2024 17:37 |
ASN Update Bot |
Added |
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