Accident Cessna 150K N6377G,
ASN logo
ASN Wikibase Occurrence # 354029
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Tuesday 28 July 1998
Time:20:53 LT
Type:Silhouette image of generic C150 model; specific model in this crash may look slightly different    
Cessna 150K
Owner/operator:Private
Registration: N6377G
MSN: 15071877
Total airframe hrs:3642 hours
Engine model:Continental O-200A
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Yorba Linda, CA -   United States of America
Phase: En route
Nature:Training
Departure airport:Fullerton, CA (KFUL)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The student was descending toward the destination airport when the engine began to run rough, then it quit altogether. The CFI took over and attempts to remedy the engine power loss were unsuccessful. During the subsequent forced landing on a city street, the aircraft collided with ground obstructions. Disassembly and examination of the engine revealed a shop rag inside the accessory case in the upper right quadrant just under the starter motor cover plate and entwined in the accessory gears. The oil suction screen was collapsed and heavily contaminated with cloth and lint fragments. The oil sump suction tube inlet was found completely plugged by rag fragments. Typical oil starvation failure signatures were noted to the internal crankshaft pins, rod ends, and bearings. The last entry in the engine logbook was dated July 16, 1998, 7 hours prior to the accident, and listed the removal and replacement of the starter.

Probable Cause: An oil starvation failure of the engine due to the mechanic's inadequate maintenance installation and quality control procedures, which resulted in a shop rag being inadvertently left inside the accessory case when the starter was changed 7 hours prior to the accident.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX98LA247
Status: Investigation completed
Duration: 2 years and 7 months
Download report: Final report

Sources:

NTSB LAX98LA247

Revision history:

Date/timeContributorUpdates
10-Mar-2024 18:03 ASN Update Bot Added

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org