ASN Wikibase Occurrence # 354038
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Date: | Sunday 26 July 1998 |
Time: | 23:00 LT |
Type: | Cessna 172M |
Owner/operator: | Flight Training, Inc. |
Registration: | N5147N |
MSN: | 17261417 |
Year of manufacture: | 1973 |
Total airframe hrs: | 9078 hours |
Engine model: | Lycoming O-320-E2D |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Franktown, CO -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Watkins, CO (KFTG) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot flew to Centennial Airport to practice touch and go landings. He departed the airport traffic pattern on an easterly heading, tuned the no. 1 navigation receiver to the Falcon Vortac, and rotated the OBS (Omni Bearing Selector) to 350 degrees. It was his intention to cross the 360 degree radial (sic, 180 degree radial), and then fly direct to the Falcon Vortac and direct to Front Range Airport. This route would avoid the Buckley ANG and Denver International Airport airspace. After he flew what he thought was an easterly heading the evidence indicates it was most probably a south-southeasterly heading) for 8 to 10 minutes and noting the CDI (Course Deviation Indicator) needle had failed to center, he made a shallow 360 degree turn and looked for recognizable landmarks. He then rotated the OBS to go direct to the Falcon Vortac, 'reset the directional gyro to the magnetic compass, making a significant correction,' and descended to 6,500 feet msl. After flying this heading for a minute, the airplane collided with terrain 11 miles southeast of Centennial Airport. Weather conditions at Centennial Airport consisted of clear skies and greater than 10 miles visibility. The pilot said it was a dark night.
Probable Cause: Flight at an altitude insufficient to clear terrain. Factors were the pilot's failure to reset or correct a precessing directional gyro, his becoming lost/disoriented, and dark night light conditions.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW98LA335 |
Status: | Investigation completed |
Duration: | 2 years and 6 months |
Download report: | Final report |
|
Sources:
NTSB FTW98LA335
History of this aircraft
Other occurrences involving this aircraft
23 February 2018 |
N5147N |
Canyon State Aero LLC |
0 |
Show Low, AZ |
|
sub |
Runway excursion |
Location
Revision history:
Date/time | Contributor | Updates |
10-Mar-2024 18:21 |
ASN Update Bot |
Added |
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