ASN Wikibase Occurrence # 354052
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Date: | Saturday 25 July 1998 |
Time: | 15:00 LT |
Type: | Enstrom F-28F |
Owner/operator: | Private |
Registration: | N8622U |
MSN: | 721 |
Year of manufacture: | 1982 |
Total airframe hrs: | 1280 hours |
Engine model: | Lycoming HIO 360 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Skwentna, AK -
United States of America
|
Phase: | Taxi |
Nature: | Unknown |
Departure airport: | , AK (KSKW) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The certificated commercial helicopter pilot was conducting a salmon survey for the State of Alaska, Department of Fish & Game. This operation required him to hover the helicopter over the stream while the passenger, a wildlife biologist employed by the State of Alaska, noted the number of fish. The pilot stated that while in a hover above the stream, he felt a slight vibration followed by a partial loss of engine power. He said that while hover taxiing the helicopter to a suitable landing area, the engine continued to lose power, and he was forced to make a downwind autorotation. He said that as the helicopter touched down, the main rotor blades flexed downward, and struck the tail boom. The helicopter's tail boom, and tail rotor gearbox sustained substantial damage. The operator reported that during a postaccident inspection of the engine, a fractured intake manifold flange was discovered on the number three cylinder assembly.
Probable Cause: A loss of engine power due to a fractured number three cylinder intake manifold flange, and the pilot's inability to maintain the proper rate of descent during the autorotation flare. A contributing factor associated with the accident was the downwind (tailwind) landing condition.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ANC98LA109 |
Status: | Investigation completed |
Duration: | 1 year and 8 months |
Download report: | Final report |
|
Sources:
NTSB ANC98LA109
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
10-Mar-2024 18:33 |
ASN Update Bot |
Added |
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