ASN Wikibase Occurrence # 354352
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Monday 8 June 1998 |
Time: | 09:15 LT |
Type: | Team Z-Max 1300 |
Owner/operator: | Private |
Registration: | N140FF |
MSN: | 1575-P |
Total airframe hrs: | 37 hours |
Engine model: | Zenoah G-50 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Buckeye, AZ -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Buckeye, AZ (KBXK) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that the engine temperature began to increase and he decided to make a precautionary landing in an open field. He later stated that he landed in that area so he could buy a drink from the local grocery store. During the landing rollout, the aircraft impacted an area of high brush. The aircraft nosed over and broke in half aft of the cockpit. The pilot holds a student pilot certificate/third-class medical dated December 3, 1993. The pilot reported that he has approximately 67 hours of total flight time, including 37 hours in the accident aircraft. An FAA inspector examined the pilot's logbook and reported that the logbook showed approximately 30 hours of flight instruction dating back to 1993, as well as a tail wheel aircraft endorsement made by a certified flight instructor approximately 5-6 months prior to the accident. The aircraft has no airworthiness certificate, nor is there an application for one. The FAA inspector examined the aircraft and reported that it was constructed of plywood and fabric. The inspector found no evidence of engine overheating. The pilot stated that he did not have the drawing plans or logbooks for the aircraft.
Probable Cause: the failure of the pilot to maintain control of the aircraft during the landing approach, and his poor in-flight planning in making an off-airport landing at an unsuitable landing area.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX98LA190 |
Status: | Investigation completed |
Duration: | 2 years and 8 months |
Download report: | Final report |
|
Sources:
NTSB LAX98LA190
Location
Revision history:
Date/time | Contributor | Updates |
11-Mar-2024 13:25 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation