Accident Mooney M20E N1306W,
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ASN Wikibase Occurrence # 354449
 
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Date:Sunday 17 May 1998
Time:22:30 LT
Type:Silhouette image of generic M20P model; specific model in this crash may look slightly different    
Mooney M20E
Owner/operator:Flight Training, Inc.
Registration: N1306W
MSN: 194
Year of manufacture:1963
Total airframe hrs:3905 hours
Engine model:Lycoming IO-360-A1A
Fatalities:Fatalities: 0 / Occupants: 3
Aircraft damage: Substantial
Category:Accident
Location:Watkins, CO -   United States of America
Phase: Taxi
Nature:Private
Departure airport:Akron, CO (KAKO)
Destination airport:(KFTG)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot said that he experienced a total electrical failure while on a night cross-country flight. He landed without incident but while taxiing along the unlit taxiway, he lost sight of the centerline stripe. The airplane went off the taxiway and down an embankment. The airport night manager said the pilot told him he would 'turn on the navigation lights, if necessary,' to warn other airplanes. Postaccident inspection disclosed that when the master switch was turned on, all electrical components functioned normally. A specific gravity check indicated the battery was fully charged. According to the operator's records, the Hobbs meter and tachometer registered 65.9 and 3903.3, respectively, when the pilot checked the airplane out. At the accident site, the Hobbs meter and tachometer registered 67.6 and 3905.1, respectively, a Hobbs meter difference of 1.7 hours and a tachometer difference of 1.8 hours. The operator said he believed the pilot had turned off the master switch in an attempt to save on rental charges. He had also received reports from other renter pilots who said the pilot had bragged about saving money by turning off the master switch. An FAA inspector said that, based on the point where the aircraft departed the taxiway and its point of impact, taxi speed was excessive.

Probable Cause: The pilot's failure to maintain visual contact with the taxiway. Factors were the pilot's disabling the electrical system by turning off the master switch, a dark night, and excessive taxi speed.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: FTW98LA222
Status: Investigation completed
Duration: 2 years and 9 months
Download report: Final report

Sources:

NTSB FTW98LA222

Location

Revision history:

Date/timeContributorUpdates
11-Mar-2024 14:33 ASN Update Bot Added

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