ASN Wikibase Occurrence # 354463
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Date: | Saturday 16 May 1998 |
Time: | 19:30 LT |
Type: | Mooney M20F |
Owner/operator: | Private |
Registration: | N6444Q |
MSN: | 670523 |
Year of manufacture: | 1967 |
Total airframe hrs: | 2500 hours |
Engine model: | Lycoming IO-360-A1A |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Telluride, CO -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Moscow, KS (KS49) |
Destination airport: | (KTEX) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:According to the pilot, he contacted the airport for a weather advisory prior to landing and was told that the winds were favoring runway 9. Prior to touchdown, he received a report on the radio that the wind had shifted to 220 degrees at 20 knots with gusts to 25 knots. The airplane touched down and as it was rolling out, the aircraft became airborne. The pilot applied full power and retracted the landing gear. He flew the aircraft approximately half way down the runway at about 20 feet above the ground, hit the ground, bounced once, then landed in a drainage ditch. Calculated density altitude at the time was 11,041 feet above mean sea level, and the angle between the runway and the wind was 130 degrees. Given the reported wind speed of 20 knots with gusts to 25 knots, the crosswind and tailwind component values fall off the wind component chart. The values at the chart limits are 12 knots and 10 knots respectively. According to Mooney Aircraft Flight Test, the demonstrated cross wind component is 13 knots and there is no demonstrated tail wind component. The propeller was destroyed, and the wings and lower fuselage sustained substantial damage.
Probable Cause: The pilot exceeded the crosswind capability performance of the aircraft, and his delayed response in initiating a go around. Factors were gusty, crosswind and tailwind conditions, and high density altitude.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW98LA224 |
Status: | Investigation completed |
Duration: | 2 years and 9 months |
Download report: | Final report |
|
Sources:
NTSB FTW98LA224
Location
Revision history:
Date/time | Contributor | Updates |
11-Mar-2024 14:40 |
ASN Update Bot |
Added |
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