ASN Wikibase Occurrence # 354700
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Date: | Thursday 19 March 1998 |
Time: | 18:30 LT |
Type: | Bell OH-58C |
Owner/operator: | Jicarilla Apache Police |
Registration: | N505JA |
MSN: | 70-15381 |
Total airframe hrs: | 6507 hours |
Engine model: | Allison T63-A-720 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Dulce, NM -
United States of America
|
Phase: | Initial climb |
Nature: | Unknown |
Departure airport: | |
Destination airport: | Dulce, NM (NM01) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot performed a preflight inspection of the helicopter for a flight from a 9,060 foot elevation. On departure, the pilot remembered the helicopter yawing nose left, and the passenger stated that the engine became quiet and the helicopter vibration seemed to stop. The pilot autorotated to the steep sloping vegetated terrain. Postimpact inspection of the engine fuel controller revealed that the PC line had disconnected from the fuel controller. The helicopter received its last annual inspection on September 18, 1997, 93 flight hours prior to the accident. The pilot reported that he had observed a Jicarilla tribal member changing navigation light bulbs on the helicopter; the same individual expressed further interest in performing maintenance on the helicopter. The maintenance organization that performed the last annual inspection did not use torque paint on the PC line B-nut, which is required by the engine manufacturer but not mandated by FARs. The pilot reported that 'because of the location of the PC line connection to the fuel controller, it would be difficult, during a normal preflight inspection, to determine if the PC line B-nut was properly torqued or if it was loose.'
Probable Cause: The partial loss of engine power due to a disconnected bleed air line to the fuel controller and the unsuitable terrain for a forced landing. Factors were the loose B-nut, the inadequate maintenance by unknown personnel, insufficient standards/requirements for the use of torque paint, and the high density altitude.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW98TA152 |
Status: | Investigation completed |
Duration: | 2 years and 11 months |
Download report: | Final report |
|
Sources:
NTSB FTW98TA152
Location
Revision history:
Date/time | Contributor | Updates |
11-Mar-2024 17:20 |
ASN Update Bot |
Added |
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