ASN Wikibase Occurrence # 354874
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Date: | Thursday 15 January 1998 |
Time: | 17:30 LT |
Type: | Bell 47G-3B-1 |
Owner/operator: | Desert Eagle Helicopters Inc. |
Registration: | N7901S |
MSN: | 6576 |
Total airframe hrs: | 3293 hours |
Engine model: | Lycoming TVO-435-B1A |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Magdalena, NM -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Unknown |
Departure airport: | Magdalena, NM |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The helicopter was being used in the Federal Government's predator control program. The pilot said he and his passenger were flying north and entered a draw. The prey they were chasing (a coyote) turned east and they flew over it at low airspeed and altitude. The pilot was having 'trouble maintaining rotor rpm.' With higher terrain in front and to his left, he elected to turn east in hopes of exiting the draw to the south. Trees and rough terrain forced him to continue eastward. The pilot found himself below a draw and he pulled collective control. This aggravated the low rpm condition, but the helicopter cleared the rim. On the other side of the rim, the ground sloped down at a 40 degree angle and the pilot tried to stretch his descent towards flatter terrain in an attempt to make a run-on landing. The helicopter impacted the terrain and was substantially damaged. The FAA inspector who went to the scene wrote, 'There is no apparent reason for the helicopter to have lost rpm. Review of the pilot records indicate only 14 hours of flight time in the last 90 days and no training in the last three years, and the last biennial flight review was almost 20 months ago.'
Probable Cause: The pilot's failure to maintain adequate main rotor rpm. A factor was a lack of recent experience in the type of operation being performed.
Accident investigation:
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| |
Investigating agency: | NTSB |
Report number: | FTW98TA099 |
Status: | Investigation completed |
Duration: | 3 years 1 month |
Download report: | Final report |
|
Sources:
NTSB FTW98TA099
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
11-Mar-2024 19:18 |
ASN Update Bot |
Added |
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