ASN Wikibase Occurrence # 354918
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Wednesday 24 December 1997 |
Time: | 00:00 LT |
Type: | Piper PA-30/A |
Owner/operator: | Private |
Registration: | N9WG |
MSN: | 30-1099 |
Year of manufacture: | 1966 |
Total airframe hrs: | 5156 hours |
Engine model: | Lycoming IO-320-C1A |
Fatalities: | Fatalities: / Occupants: 3 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Hastings, NE -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Cheyenne, WY (KCYS) |
Destination airport: | (KHSI) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The flight had originally departed from Nampa, Idaho, at 0830 mountain standard time (mst) with Mountain Home, Idaho, as a stopover airport, and Hastings, Nebraska, as the intended final destination airport. The pilot departed Cheyenne, Wyoming, about 1940 mst. At 2224 central standard time (cst), the pilot was briefed that the weather at Hastings indicated winds at 080 degrees at 4 knots, one quarter mile visibility, freezing fog, a few clouds at 100 feet, 4,200 foot overcast, temperature minus 2 degrees C, dew point minus 2 degrees C, and altimeter 29.87. At 2227, the pilot reported, 'Whiskey golf, we're gonna shoot an approach into Hastings, ah, if it's no good we'll, ah, do a missed and go somewhere else.' At 2250, the pilot reported, 'ah, Missed approach. I (want to) try it again.' The pilot received clearance to fly a second approach. At 2300 cst, the aircraft impacted an irrigation tower and wheel assembly that was located about 1/2 mile west of the airport. Both propellers indicated blade twist and chordwise scratching. The right seat passenger reported that the pilot had not indicated there was anything wrong with the airplane during the flight, she remembered that the pilot flew the second approach down to 2,300 feet or 2,350 feet on the altimeter and started to pull up on the airplane's yoke. The field elevation was 1,961 feet. The MDA was 2,360 feet. The altimeter was set at 29.84. During the flight, there had been no indications of altimeter error when the pilot was in contact with ATC.
Probable Cause: The pilot's improper IFR procedure, by which he failed to maintain minimum descent altitude. Fog, a low ceiling, and night condition were a contributing factor.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI98LA072 |
Status: | Investigation completed |
Duration: | 1 year and 9 months |
Download report: | Final report |
|
Sources:
NTSB CHI98LA072
History of this aircraft
Other occurrences involving this aircraft
23 December 1997 |
N9WG |
T.C.Bundy |
1 |
1/2 mile W of Hastings Municipal Airport, Hastings, Nebraska |
|
w/o |
Location
Revision history:
Date/time | Contributor | Updates |
12-Mar-2024 06:06 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation