ASN Wikibase Occurrence # 354977
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Date: | Sunday 30 November 1997 |
Time: | 19:42 LT |
Type: | Piper PA-24-250 |
Owner/operator: | Private |
Registration: | N6661P |
MSN: | 24-1784 |
Year of manufacture: | 1960 |
Total airframe hrs: | 5151 hours |
Engine model: | Lycoming O-540-A1C5 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Lubbock, TX -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | San Antonio, TX (KSAT) |
Destination airport: | (KLBB) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During the initial takeoff departure climb, the gear would not retract and the pilot returned to the airport where a mechanic examined the gear, serviced the struts, and performed a retraction test (gear were extended and retracted 3 consecutive times). Subsequently, the flight departed on the cross country flight with a planned refueling stop. During the approach, the gear would not extend. The pilot maneuvered in the area and performed the emergency gear extension procedures; however, the gear would not go beyond 1/2 extension. During the final approach to the runway, the pilot shut down the engine and the airplane landed short of the runway. The FAA inspector and a mechanic found that the 'slide tubes on the main gear had accumulated a lot of dirt causing some binding on their normal operation. This binding consistently caused the gear electric motor circuit breaker to pop.' The gear could be extended manually by the FAA inspector and the mechanic. Flight time since the last annual inspection was 57 hours.
Probable Cause: The inadequate maintenance of the landing gear assembly by maintenance personnel resulting in a partial gear extension, and the pilot's misjudgment of a proper touchdown point to intentionally shut down the engine resulting in the airplane landing short of the runway. A factor was the soft terrain.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW98LA060 |
Status: | Investigation completed |
Duration: | 11 months |
Download report: | Final report |
|
Sources:
NTSB FTW98LA060
Location
Revision history:
Date/time | Contributor | Updates |
12-Mar-2024 06:38 |
ASN Update Bot |
Added |
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