Accident Mooney M20F N7433V,
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ASN Wikibase Occurrence # 355109
 
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Date:Sunday 19 October 1997
Time:02:16 LT
Type:Silhouette image of generic M20P model; specific model in this crash may look slightly different    
Mooney M20F
Owner/operator:Texas A&m Flying Club Inc.
Registration: N7433V
MSN: 22-1210
Total airframe hrs:3871 hours
Engine model:Lycoming IO-360-A1A
Fatalities:Fatalities: 0 / Occupants: 4
Aircraft damage: Substantial
Category:Accident
Location:College Station, TX -   United States of America
Phase: Unknown
Nature:Private
Departure airport:Oklahoma City, OK
Destination airport:(KCLL)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The night cross country flight originated at Manhattan, Kansas, where the four college students aboard the airplane attended a Kansas State-Texas A&M football game. The flight had landed at Oklahoma City for fuel near midnight. The pilot reported that he had visual contact with the Easterbrook Field Airport when 15 miles north of the airport. After obtaining the weather, he initiated a descent for a straight-in approach to Runway 16. The pilot added 'while on short final he felt that his rate of descent was too steep' so he elected to execute a go-around when the airplane was approximately 40 feet above the runway. The pilot reported that 'the airplane stalled after he applied full power and retracted the landing gear and flaps.' In the enclosed statement, under the heading of 'Other General Observations,' the pilot stated that he was extremely fatigued due to the 20 hour day, the 8.5 hour flight-day and the chronic fatigue from being a college student. He also noted that he felt extreme pressure from the passengers to get back to Texas ('get-there-itis'). The pilot also stated that this was only his second night landing in the airplane and he considered himself 'to have low time' in the airplane.

Probable Cause: The pilot's failure to maintain airspeed during a go-around. Factors were :the pilot's premature retraction of the flaps, his lack of total experience in the airplane, the dark night illumination, pilot fatigue, and pressure induced by the passengers to complete the night flight.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: FTW98LA018
Status: Investigation completed
Duration: 6 months
Download report: Final report

Sources:

NTSB FTW98LA018

Location

Revision history:

Date/timeContributorUpdates
12-Mar-2024 08:25 ASN Update Bot Added

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