ASN Wikibase Occurrence # 355152
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Date: | Monday 6 October 1997 |
Time: | 13:30 LT |
Type: | Beechcraft G35 |
Owner/operator: | Private |
Registration: | N129B |
MSN: | D-4433 |
Total airframe hrs: | 5439 hours |
Engine model: | Continental E-225-8 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Poplar Grove, IL -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Janesville, WI (KJVL) |
Destination airport: | (C77) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that he was cruising at 4,000 feet msl in clear sky conditions with smooth air, then he initiated a descent. He said that while descending through about 3,200 feet msl at 185 mph with a 5 degree nose down attitude and 15 degree left turn, the control yoke started oscillating fore and aft about 1/2 inch. The oscillations increased to about 1 inch fore and aft, and the airplane experienced 3 or 4 'solid jolts.' After about 5 seconds, the pilot reduced power, and the vibrations stopped. He continued to his destination and landed uneventfully. According to the Pilot Operating, the airplane's never exceed airspeed (Vne) was 202 mph. The maximum cruise airspeed (Vno), was 175 mph. Inspection of the airplane revealed that the aft fuselage received extensive damage between fuselage station (FS) 256.9 and the 233.5 bulkhead. The longerons were bent downward with a permanent 2.5 to 3 inch bend. The left and right side fuselage panels below the stabilizers exhibited 45 degree buckling from the bottom of the FS 256.9 bulkhead to forward of the stabilizer cuffs. The bottom fuselage panel forward of the 256.9 bulkhead had popped rivets and torn skin. There were three creases in the right stabilizer. No pre-existing cracks were found on the longerons. The ruddervators were properly balanced.
Probable Cause: flutter for an undetermined reason, which resulted in structural damage to the aft fuselage.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI98FA017 |
Status: | Investigation completed |
Duration: | 2 years and 4 months |
Download report: | Final report |
|
Sources:
NTSB CHI98FA017
Location
Revision history:
Date/time | Contributor | Updates |
12-Mar-2024 08:51 |
ASN Update Bot |
Added |
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