ASN Wikibase Occurrence # 355238
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Date: | Friday 19 September 1997 |
Time: | 19:48 LT |
Type: | Cessna 402C |
Owner/operator: | Ocean Wings Inc |
Registration: | N6879Y |
MSN: | 402C0612 |
Year of manufacture: | 1981 |
Total airframe hrs: | 14200 hours |
Engine model: | Continental TSIO-520 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Nantucket, MA -
United States of America
|
Phase: | Approach |
Nature: | Ferry/positioning |
Departure airport: | Hyannis, MA (KHYA) |
Destination airport: | (KACK) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot-in-command (PIC) and pilot/passenger (copilot) diverted to another airport prior to their destination because of low visibility at the destination airport. The visibility was low due to fog, but the pilots decided to continue to their original destination after they had deplaned their passengers. At the final destination, the PIC could not land from the first ILS approach due to poor visibility and attempted a second approach. He said that after the second approach, he had the runway environment in sight, but decided to go around because '... something didn't feel right.' The co-pilot said he got disoriented and confused, and called for a go-around. However, the airplane struck the ground immediately thereafter. Rescue workers reported difficulty finding the airplane due to poor visibility. They estimated the visibility at less than 25 feet. Weather reported at the time of the accident was: measured ceiling 100 feet obscured, 1/4 mile visibility with fog. The temperature and dew point were 65 degrees. Winds were from 180 degrees at 6 knots.
Probable Cause: the pilot's delayed decision to perform a go-around (missed approach). Related factors were: darkness, low ceiling, fog, and disorientation of the flight crew, while making the approach in conditions of limited visibility.
Accident investigation:
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| |
Investigating agency: | NTSB |
Report number: | NYC97LA183 |
Status: | Investigation completed |
Duration: | 1 year 1 month |
Download report: | Final report |
|
Sources:
NTSB NYC97LA183
History of this aircraft
Other occurrences involving this aircraft
20 April 1985 |
N6879Y |
Aero Coach Aviation Int'l,inc. |
0 |
West Palm Beach, FL |
|
min |
Revision history:
Date/time | Contributor | Updates |
12-Mar-2024 09:49 |
ASN Update Bot |
Added |
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