ASN Wikibase Occurrence # 355363
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Thursday 21 August 1997 |
Time: | 14:35 LT |
Type: | Rockwell S-2R Thrush Commander |
Owner/operator: | Private |
Registration: | N4893X |
MSN: | 2078R |
Engine model: | P&W R-1340-AN1 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Columbus, NM -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Agricultural |
Departure airport: | Deming, NM (KDMN) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane impacted terrain following a loss of engine power while maneuvering. The pilot stated 'on the final pass [he] pulled up out of the field and initiated a turn towards Deming, when an object came through the right corner windshield striking [him] in the head,' rendering him unconscious. A witness who was approximately 1 mile from the accident site stated that he saw the airplane 'flying straight and then nose into the ground.' The witness did not hear any engine noises. Several workers, in a nearby field, reported that they observed the airplane pull out of the field and start to turn, when the engine quit. The owner examined the engine and determined that the exhaust side rocker box and exhaust valve mechanism had broken off the number 7 cylinder. There was a 'deep groove' on the back side of a propeller blade. The owner stated that the rocker box could have been ejected from the engine and contacted a propeller blade which deflected the rocker box into the cabin.
Probable Cause: a loss of engine power due to failure of an exhaust side rocker box and valve mechanism, and pilot incapacitation due to loss of consciousness after being struck in the head by parts separating from the engine.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW97LA322 |
Status: | Investigation completed |
Duration: | 1 year and 2 months |
Download report: | Final report |
|
Sources:
NTSB FTW97LA322
Revision history:
Date/time | Contributor | Updates |
12-Mar-2024 11:11 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation