ASN Wikibase Occurrence # 355420
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Date: | Saturday 9 August 1997 |
Time: | 13:35 LT |
Type: | Cessna 150G |
Owner/operator: | Tom King Aerial Enterprises |
Registration: | N3084S |
MSN: | 15066984 |
Year of manufacture: | 1967 |
Total airframe hrs: | 3421 hours |
Engine model: | Lycoming O-360-A4M |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Palos Verdes, CA -
United States of America
|
Phase: | En route |
Nature: | Unknown |
Departure airport: | Chino, CA (KCNO) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The aircraft had been modified with installation of: 1) a Lycoming O-360 engine; 2) an 18-gallon auxiliary fuel tank in the baggage compartment; and 3) a Cessna 172 type main fuel selector capable of selecting right, left, both, and off positions. The auxiliary tank was plumbed to pump fuel through an electric pump and an on-off fuel valve into the right wing tank. The fuel quantity sending unit was wired through a toggle switch to the right wing tank fuel gage; the switch could select either the right wing or auxiliary tank for gage display. The fuel system operating procedures specify that the pilot is to use fuel from the right wing tank first for 1 hour, then transfer fuel from the auxiliary tank. The pilot reported that after picking up the banner he climbed on a westerly heading on both tanks. Approximately 15 minutes later, the pilot switched to the right tank. He reported that 1 1/2 hour later he switched to the auxiliary tank. The right tank fuel gage read 1/4 full. At this point the engine stopped, and he switched back to both tanks in an attempt to restart the engine. The pilot reported that the attempted engine restart was unsuccessful and he had to ditch the aircraft in the ocean. After the aircraft was recovered, 2 gallons of fuel were drained from right tank, and 18-20 gallons of fuel were drained from the left tank. In a verbal statement to FAA inspectors, the pilot reported that he forgot to switch the fuel selector.
Probable Cause: Loss of engine power due to fuel starvation and the pilot's mismanagement of the aircraft's fuel supply.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX97LA278 |
Status: | Investigation completed |
Duration: | 1 year and 3 months |
Download report: | Final report |
|
Sources:
NTSB LAX97LA278
History of this aircraft
Other occurrences involving this aircraft
27 June 2020 |
N3084S |
High Exposure Inc |
0 |
off Surf City, Ocean County, NJ |
|
sub |
Location
Revision history:
Date/time | Contributor | Updates |
12-Mar-2024 11:49 |
ASN Update Bot |
Added |
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