ASN Wikibase Occurrence # 355449
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Date: | Sunday 3 August 1997 |
Time: | 18:15 LT |
Type: | Cessna 172 RG |
Owner/operator: | Mercury Flight Center |
Registration: | N9647B |
MSN: | 172RG0943 |
Total airframe hrs: | 2854 hours |
Engine model: | Lycoming O-360-F1A6 |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Quinton, VA -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Norfolk, VA (KORF) |
Destination airport: | Richmond, VA (KRIC) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot was in cruise flight when he discovered that neither the radios nor the fuel gauges were operating. The airplane had flown approximately one hour on full fuel tanks. The pilot chose to make a precautionary landing at an airport 10 miles prior to his destination. The pilot stated that he lowered the landing gear '...and received what I thought was a safe gear indication.' Two witnesses stated they saw the airplane over the runway with the main landing gear out of the wheel wells, but not completely down and locked. Before they could advise the pilot over the radio, the airplane touched down. After touchdown, the main gear collapsed and the airplane departed the left side of the runway. In a written statement, the pilot said, 'During the flight, I didn't notice the low voltage light on the ammeter.' The examination of the airplane included a check of the battery voltage which showed 19.5 volts. This reading immediately dropped to 9 volts when the master switch was turned on. The gear warning horn operated when the throttle was retarded. The low voltage light illuminated, however it was difficult to see without shielding it from the sunlight. The battery was placed on a charger and the engine was started. The ammeter showed a positive charge, indicating the alternator was operating.
Probable Cause: The pilot's failure to identify an unsafe landing gear condition. A factor in the accident was the loss of electrical power.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | NYC97LA158 |
Status: | Investigation completed |
Duration: | 4 years |
Download report: | Final report |
|
Sources:
NTSB NYC97LA158
Location
Revision history:
Date/time | Contributor | Updates |
12-Mar-2024 12:08 |
ASN Update Bot |
Added |
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