Accident Bellanca 17-30 N70EC,
ASN logo
ASN Wikibase Occurrence # 355627
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Friday 4 July 1997
Time:11:30 LT
Type:Silhouette image of generic BL17 model; specific model in this crash may look slightly different    
Bellanca 17-30
Owner/operator:Private
Registration: N70EC
MSN: 30193
Engine model:Continental IO-520-O
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Prescott, AZ -   United States of America
Phase: Unknown
Nature:Private
Departure airport:Quartzsite, AZ (2L3)
Destination airport:(KPRC)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The aircraft was entering the airport for runway 21 when the tower cleared him to land on runway 30 instead. The pilot said he attempted to add power to extend his approach when the engine seemed to drop to idle. In an attempt to land on runway 21 he extended his landing gear but touched down approximately 60 feet short of the runway. The pilot stated he had 45 gallons of fuel in the airplane before takeoff. It was determined during the postcrash aircraft examination that the fuel selector had no noticeable detent when it was moved from position to position. Additionally, the placards were not legible on the fuel selector. There was no visible fuel found in the left auxiliary tank, and only a trace in the right auxiliary tank. A stick test determined that there was approximately 4 inches of fuel in the right and left main tank. During the postaccident examination of the engine, there were no abnormalities found that would have prevented the engine from being run.

Probable Cause: The pilot's improper placement of the unmarked fuel selector valve to off which resulted in fuel starvation. A factor in the accident was the pilot's lack of total experience in this model aircraft.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX97LA238
Status: Investigation completed
Duration: 10 months
Download report: Final report

Sources:

NTSB LAX97LA238

Location

Revision history:

Date/timeContributorUpdates
12-Mar-2024 13:59 ASN Update Bot Added

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org