ASN Wikibase Occurrence # 355755
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Date: | Friday 13 June 1997 |
Time: | 13:00 LT |
Type: | Air Tractor AT-502A |
Owner/operator: | Private |
Registration: | N248LF |
MSN: | |
Engine model: | P&W PT6A-45A |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Chesterville, TX -
United States of America
|
Phase: | Landing |
Nature: | Agricultural |
Departure airport: | |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:After landing about 200 feet beyond the approach end of the 2,600 foot runway, the pilot attempted to apply reverse power, 'but did not receive any reversing action.' After attempting full reverse, 'the prop sounded like it was going to flat pitch.' In an attempt to 'go around,' the pilot pushed the power lever to full forward, but did not get any response. Another attempt was made to apply reverse with no response. Approaching the departure end of the runway, the pilot applied left brake and intentionally ground looped the airplane to avoid hitting parked trucks adjacent to the end of the runway. Subsequently, the right main landing gear sheared and the airplane skidded into a ditch. External examination of the engine, engine accessory gearbox, and propeller assemblies did not reveal any obvious preimpact anomalies. No oil leaks were found in the propeller piston or the propeller governor assembly. All cockpit power control quadrant linkages were intact, and the reverse detent on the thrust lever operated normally when cycled. Teardown examination of the propeller assembly did not reveal any defects. The propeller governor did not show any abnormality during functional bench tests.
Probable Cause: an undetermined malfunction/failure of the propeller reversing system.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW97LA225 |
Status: | Investigation completed |
Duration: | 4 months |
Download report: | Final report |
|
Sources:
NTSB FTW97LA225
Location
Revision history:
Date/time | Contributor | Updates |
12-Mar-2024 15:18 |
ASN Update Bot |
Added |
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