ASN Wikibase Occurrence # 356239
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Date: | Tuesday 18 February 1997 |
Time: | 15:15 LT |
Type: | Piper PA-32R-300 |
Owner/operator: | Private |
Registration: | N4477F |
MSN: | 32R-7680449 |
Year of manufacture: | 1976 |
Total airframe hrs: | 3000 hours |
Engine model: | Lycoming I0-540-K1G5D |
Fatalities: | Fatalities: 0 / Occupants: 5 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Salida, CO -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | (0V2) |
Destination airport: | Tyler, TX (KTYR) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that during takeoff roll the aircraft accelerated to 60 MPH like it 'normally' does; however, it took 'longer than normal to accelerate to 80 MPH.' The aircraft appeared to 'lift off fine, but it didn't seem to climb as well as he would have liked.' He put the gear up and about 30 to 35 feet above the runway he lowered the aircraft's nose to accelerate to the best angle of climb airspeed. Instead of accelerating and continuing to climb, the aircraft began to descend. He 'cut the power,' and as the airplane touched down, the nose and left main landing gear collapsed. The airplane has automatic extending landing gear. The pilot did not use any flaps for the takeoff. The pressure altitude at the time of the accident was 7,489 feet and the temperature was 48 degrees Fahrenheit. The performance data derived for these conditions would be off of the chart. In the same section, there is a warning that, 'Performance information derived by extrapolation beyond the limits shown on the charts should not be used for flight planning purposes.' This was the pilot's third takeoff from a high altitude airport. Runway 24 rises 1.9 degrees, which equates to a 117 foot rise.
Probable Cause: The airplane's performance being exceeded due to the pilot's inadequate preflight planning. Factors were the uphill runway, high density altitude, and the pilot's lack of experience performing takeoffs from a high altitude airport.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW97LA107 |
Status: | Investigation completed |
Duration: | 6 months |
Download report: | Final report |
|
Sources:
NTSB FTW97LA107
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
12-Mar-2024 20:31 |
ASN Update Bot |
Added |
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