ASN Wikibase Occurrence # 356287
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Date: | Monday 27 January 1997 |
Time: | 11:15 LT |
Type: | Cessna U206D |
Owner/operator: | Red Baron Aviation, Inc. |
Registration: | N72074 |
MSN: | U206-1275 |
Year of manufacture: | 1969 |
Total airframe hrs: | 5125 hours |
Engine model: | Continental IO-520-A |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Tampa, FL -
United States of America
|
Phase: | Initial climb |
Nature: | Unknown |
Departure airport: | (KTPA) |
Destination airport: | Miami, FL (KTMB) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot had flown the airplane once around the traffic pattern earlier in the morning with no discrepancies noted following removal and reinstallation of 4 of the 6 cylinders several days earlier. He then flew the airplane on a short positioning flight also with no discrepancies noted. The flight then departed on the chartered cargo flight and shortly after takeoff, the engine experienced a partial then complete loss of power. With unsuitable terrain ahead the pilot ditched the airplane. Following recovery of the airplane examination of the engine revealed the crankshaft was failed aft of the No. 2 main bearing due to fatigue then overload. Fretting was noted on both crankcase halves at the No. 2 main bearing saddle and the associated bearing was broken, extruded, and the bearing saddle was also extruded. Also, the No. 3 main bearing halves were found to be shifted. Review of the maintenance records revealed that overhauled cylinders were installed at all positions in August of 1996. The engine had been operated for 423 hours since at the time of the accident.
Probable Cause: Inadequate torque of the cylinder base nuts and through bolt nuts by company maintenance personnel which allowed movement of the crankcase halves. As a result the No. 2 main bearing failed which allowed excessive movement of the crankshaft resulting in fatigue failure of the crankshaft. Contributing to the accident was unsuitable terrain encountered by the pilot during the forced landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA97LA076 |
Status: | Investigation completed |
Duration: | 1 year |
Download report: | Final report |
|
Sources:
NTSB MIA97LA076
Location
Revision history:
Date/time | Contributor | Updates |
12-Mar-2024 20:59 |
ASN Update Bot |
Added |
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