ASN Wikibase Occurrence # 356368
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Date: | Tuesday 31 December 1996 |
Time: | 11:33 LT |
Type: | Cessna 182P |
Owner/operator: | Torger James Totusek |
Registration: | N9003M |
MSN: | 18264638 |
Year of manufacture: | 1976 |
Total airframe hrs: | 2000 hours |
Engine model: | Continental O-470S |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Fullerton, CA -
United States of America
|
Phase: | Initial climb |
Nature: | Training |
Departure airport: | (KFUL) |
Destination airport: | Santa Barbara, CA |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:According to both pilots, following receipt of their departure release and takeoff clearance, the aircraft took off and climbed to approximately 500 feet agl when the engine smoothly lost power. The engine power returned briefly, dropped off, surged, and then quit altogether. The pilot flying the aircraft attempted to return to the runway, but had insufficient altitude and collided with a fence at the approach end of runway 24. That pilot reported that a preflight had been conducted per the POH and that no abnormalities were found. The aircraft was examined by an FAA airworthiness inspector who reported finding the gascolator bowl half full of water and the carburetor bowl completely full of water. No water was found in either fuel tank when the sump drains were checked. The engine was then started and run for a 10-minute period with no abnormalities noted. Additionally, the FAA inspector found that the left tank fuel cap O-ring was deteriorated, with rust and corrosion present below the level of the O-ring. The aircraft is parked outside on the ramp. Heavy periods of rainfall occurred during the week prior to the accident flight. An annual inspection was completed on the aircraft 1 month and 3 flight hours prior to the accident.
Probable Cause: Fuel system water contamination due to the failure of both pilots to purge all water from the fuel system prior to departure. Contributing factors were: failure of the mechanic conducting the recent annual inspection to identify and replace a deteriorated fuel cap O-ring.
Accident investigation:
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| |
Investigating agency: | NTSB |
Report number: | LAX97LA080 |
Status: | Investigation completed |
Duration: | 1 year 1 month |
Download report: | Final report |
|
Sources:
NTSB LAX97LA080
History of this aircraft
Other occurrences involving this aircraft Revision history:
Date/time | Contributor | Updates |
13-Mar-2024 06:30 |
ASN Update Bot |
Added |
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