Accident Beechcraft B19 N5102R,
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ASN Wikibase Occurrence # 356527
 
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Date:Wednesday 30 October 1996
Time:11:15 LT
Type:Beechcraft B19
Owner/operator:Ari Ben Aviator Inc.
Registration: N5102R
MSN: MB636
Total airframe hrs:14360 hours
Engine model:Lycoming O-360-A4D
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Mckinney, TX -   United States of America
Phase: Landing
Nature:Training
Departure airport:(KTKI)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The student pilot was endorsed for repeated solo flights and was performing a touch-and-go landing on runway 17. He reported that on final approach, he maintained an airspeed of 70 to 75 knots with full flaps, and that the approach path followed the VASI. He said that while landing, the airplane touched down about midfield, and subsequently, with all 3 wheels on the runway, he retracted the flaps, pushed the carburetor heat to 'COLD,' and reached for the throttle to apply power for the departure. The student pilot stated that at this point, 'the airplane brakes were binding, the airplane exited the left side of the runway, continued through the grass, and stopped after the left wing struck a tree.' An FAA inspector, who examined the accident site, found that the student was using a personal fold-up seat/cushion that was about 5 inches thick. During the investigation, the inspector had the student pilot sit in the airplane. The inspector observed that the 'extra height caused his knees to contact the lower part of the instrument panel and hindered his ankle movement for proper rudder and brake action.' The inspector did not find 'any evidence of brake problems.'

Probable Cause: the pilot's inadequate preflight planning/preparation, by selecting a seat/cushion that would not allow adequate knee clearance and ankle movement in the cockpit, which was subsequently attributed to the pilot's failure to maintain directional control during the landing roll.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: FTW97LA031
Status: Investigation completed
Duration: 9 months
Download report: Final report

Sources:

NTSB FTW97LA031

Location

Revision history:

Date/timeContributorUpdates
13-Mar-2024 08:07 ASN Update Bot Added

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