Accident RotorWay Exec 162F N711KN,
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ASN Wikibase Occurrence # 356528
 
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Date:Tuesday 29 October 1996
Time:08:37 LT
Type:Silhouette image of generic EXEC model; specific model in this crash may look slightly different    
RotorWay Exec 162F
Owner/operator:Private
Registration: N711KN
MSN: 6072
Total airframe hrs:40 hours
Engine model:Rotorway 162F
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Haines, AK -   United States of America
Phase: En route
Nature:Training
Departure airport:, AK (KHNS)
Destination airport:Juneau, AK (JNU)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The certificated private airplane pilot, the sole occupant & holder of a solo endorsement for helicopters, was beginning a cross-country flight in an experimental homebuilt helicopter. After takeoff, he heard a sharp bang & observed smoke in the cockpit. He declared an emergency, entered an autorotation, & selected an emergency landing area on a beach, but the area was covered with large boulders. During the flare & landing, the engine responded momentarily, when the pilot raised the collective pitch control, but the engine did not have sufficient power to hover. The helicopter sustained damage to the landing gear skids, the tail rotor, & the tail boom structure adjacent to the tail rotor assembly. An exam revealed the engine compartment was coated with engine coolant. The air intake filter was saturated with coolant, & 1 electronic ignition system was rendered inoperative from coolant saturation. A pressure test of the coolant system revealed a leak & spraying of coolant from a coolant pump manifold fitting. The pilot indicated the fitting had a rubber hose attached by a clamp, & coolant was leaking at the attach point. Also, he said the hose had been installed with excessive tension at the fitting due to it being 1/2 inch too short. He had accrued 47 hrs in helicopters.

Probable Cause: a leaking coolant hose that saturated the induction air filter and one electronic ignition system with coolant. Unsuitable terrain for a forced landing was a related factor in the accident.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ANC97LA005
Status: Investigation completed
Duration: 1 year and 5 months
Download report: Final report

Sources:

NTSB ANC97LA005

Location

Revision history:

Date/timeContributorUpdates
13-Mar-2024 08:07 ASN Update Bot Added

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