ASN Wikibase Occurrence # 35661
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Date: | Thursday 9 July 1992 |
Time: | 08:50 LT |
Type: | Cessna T210N |
Owner/operator: | Edward Curtis |
Registration: | N6483C |
MSN: | 21063900 |
Total airframe hrs: | 2894 hours |
Engine model: | CONTINENTAL TSIO-520-R |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Superior, AZ -
United States of America
|
Phase: | En route |
Nature: | Executive |
Departure airport: | Safford, AZ (KSAD) |
Destination airport: | Phoenix, AZ (KPHX) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE CERTIFICATED PRIVATE PILOT, THE SOLE OCCUPANT, WAS ON A CROSS COUNTRY BUSINESS FLIGHT WHEN THE ENGINE QUIT. THE PILOT MADE A FORCED LANDING ABOUT 250 FEET SHORT OF A DIRT AIRSTRIP. THE AIRPLANE WAS DESTROYED BY IMPACT AND A POST IMPACT FIRE, AND THE PILOT WAS FATALLY INJURED. EXAMINATION OF THE ENGINE REVEALED A BROKEN CRANKSHAFT ON THE CRANKCHEEK ADJACENT TO THE NUMBER 1 CYLINDER. THE CRANKSHAFT HAD BEEN REPLACED 42 HOURS PRIOR TO THE ACCIDENT. THE CRANKSHAFT WAS SUPPLIED FROM AN ENGINE WITH AN ACCUMULATED TOTAL TIME OF ABOUT 1,000 HOURS OF OPERATION THAT HAD PREVIOUSLY SUSTAINED A SEPARATION OF THE NUMBER 1 CYLINDER FROM THE ENGINE CASE. AFTER AN INSPECTION, THE CRANKSHAFT WAS DETERMINED TO BE SERVICEABLE AND INSTALLED IN THE ACCIDENT AIRPLANE'S ENGINE. METALLURGICAL EXAMINATION REVEALED A HIGH CYCLE FATIGUE FAILURE CONSISTENT WITH SURFACE INITIATED CRACKING. A METALLURGICAL REPORT INDICATED THAT SURFACE CRACKING WOULD NOT BE EXPECTED IN THE AREA OF FAILURE UNLESS PRIOR DAMAGE TO THE SURFACE HAD OCCURRED.
Probable Cause: AN INADEQUATE MAJOR ENGINE OVERHAUL PROCEDURE, DURING WHICH PREVIOUS CRANKSHAFT DAMAGE WAS NOT DETECTED. CONTRIBUTING TO THE ACCIDENT WAS A SURFACE INITIATED FATIGUE FAILURE OF THE ENGINE CRANKSHAFT.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX92FA289 |
Status: | Investigation completed |
Duration: | 11 months |
Download report: | Final report |
|
Sources:
NTSB LAX92FA289
Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:22 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
10-Apr-2024 19:41 |
ASN Update Bot |
Updated [Time, Other fatalities, Departure airport, Destination airport, Source, Narrative, Accident report] |
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