ASN Wikibase Occurrence # 356622
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Date: | Tuesday 1 October 1996 |
Time: | 09:00 LT |
Type: | Continental Copters El Tomcat Mk V-A |
Owner/operator: | Private |
Registration: | N7MH |
MSN: | MHTE-7 |
Engine model: | Lycoming VO-435-A1F |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Lafayette, LA -
United States of America
|
Phase: | Take off |
Nature: | Agricultural |
Departure airport: | |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that he and his groundcrew were preparing to commence an aerial application job for a farmer who was reportedly 'anxious' to get the job underway. The helicopter was transported to the job site on a trailer from which it was normally operated. After a preflight, the pilot prepared to take off from the trailer. Upon lift-off, the rear portion of the left skid became 'snagged' on the left rear tiedown. According to a witness and the pilot, the aircraft 'pitched up, rolled left', and at 'least one of the main rotor blades struck the ground.' Subsequently, the skid broke loose from the tie down, and the nose pitched down and impacted the ground. During this sequence, the tail boom separated from the helicopter. The pilot reported that he and his groundcrew were fatigued when they arrived on the job. During a 168 day time period, he had flown over 400 hours, and had spent approximately 656 hours driving to jobs. He reported his normal work day to be 0500 to 2300 (allowing 6 hours for sleep). The pilot stated that he needed 8 hours of sleep on average to feel fully rested.
Probable Cause: the pilot's failure to ensure a proper preflight and the groundcrew's failure to remove the tiedown. Factors were pilot and groundcrew fatigue.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW97LA001 |
Status: | Investigation completed |
Duration: | 7 months |
Download report: | Final report |
|
Sources:
NTSB FTW97LA001
Revision history:
Date/time | Contributor | Updates |
13-Mar-2024 09:12 |
ASN Update Bot |
Added |
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