ASN Wikibase Occurrence # 356730
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Date: | Friday 6 September 1996 |
Time: | 18:45 LT |
Type: | Cessna 150L |
Owner/operator: | Ace Aviation |
Registration: | N6632G |
MSN: | 15072132 |
Total airframe hrs: | 4636 hours |
Engine model: | Continental O-200 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Hope, ME -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Portland, ME (KPWM) |
Destination airport: | Belfast, ME (KBST) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:While returning from a round trip, cross-country flight, the engine lost power. The pilot was unable to restart the engine, & performed a forced landing to a grass field. During the landing, the airplane nosed over and was damaged. The HOBBS meter reading indicated the airplane had been operated for 5.4 hrs. The pilot said he departed knowing he was pushing the envelope for fuel, but he figured he had enough to get home, since the left tank fuel quantity was above 1/4 & the right tank fuel quantity showed above zero. The airplane had a supplemental type certificate for use of automotive gasoline. The pilot said he did not refuel the airplane during the trip because his flight instructor told him to use automotive gasoline only. He was told automotive gasoline was unavailable at his points of landing; however, aviation gasoline was available. The pilot was not aware of the compatibility between automotive & aviation gasoline. The airplane was examined by an FAA Inspector; according to his report, fuel was found in a line between the gascolator & carburetor. At least 1 gal of fuel was drained from the right fuel tank & 2 or 3 cups of fuel leaked out of the left fuel tank. An undetermined amount of fuel was observed pulsing out of the fuel vent tube. No preimpact failure of the engine or airframe was reported. The airplane's fuel capacity was 26 gal, of which 3.5 gal were unusable.
Probable Cause: inadequate preflight, by not refueling the airplane during an en route stop, which led to fuel exhaustion, loss of engine power, and a subsequent forced landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | IAD96LA144 |
Status: | Investigation completed |
Duration: | 1 year and 12 months |
Download report: | Final report |
|
Sources:
NTSB IAD96LA144
Revision history:
Date/time | Contributor | Updates |
13-Mar-2024 10:17 |
ASN Update Bot |
Added |
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